ASN Wikibase Occurrence # 39684
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Date: | Monday 24 July 1995 |
Time: | 07:50 LT |
Type: | Beechcraft 35F |
Owner/operator: | Gary E. Balke |
Registration: | N4288B |
MSN: | D-4219 |
Year of manufacture: | 1955 |
Total airframe hrs: | 4533 hours |
Engine model: | CONTINENTAL E-225-8 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mt Dora, FL -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | (X55) |
Destination airport: | (KOSH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and his passenger were en route to Oshkosh, Wisconsin, to attend the Experimental Aircraft Association annual meeting. They had intended to camp in tents while at the meeting. The pilot departed his home earlier in the morning, and flew to the Mid-Florida Airport to pick up a passenger. After arriving, the pilot told witnesses that during the flight, the airplane's center of gravity was aft, and he had to use a lot of forward trim to maintain level flight. The pilot and passenger hurriedly loaded the passenger's baggage on board the airplane, without weighing the baggage, and attempted to depart. The takeoff roll was longer than normal, and the airplane climbed to about 300 feet. The airplane began a right turn, then it entered a left bank, which continued to steepen. The airplane then entered a steep descent and crashed in a lake. Weight and balance calculations showed the airplane's gross weight (GW) was 2765 pounds, and its center-of-gravity (CG) was at 85.4 inches. Its maximum certificated GW for takeoff was 2757.5 pounds, and its aft CG limit for that weight was 85.1 inches.
Probable Cause: the pilot's inadequate preflight planning/preparation by allowing the airplane's weight and balance to be exceeded, and his failure to maintain control of the airplane, while turning after takeoff, which resulted in an inadvertent stall.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL95FA142 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB ATL95FA142
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2024 13:22 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Destination airport, Source, Narrative, Category, Accident report] |
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