| Date: | Monday 29 July 2024 |
| Time: | 21:30 |
| Type: | Piper PA-32R-301T Saratoga II TC |
| Owner/operator: | Private |
| Registration: | N5343C |
| MSN: | 3257255 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Myrtle Beach-Grand Strand Airport (CRE/KCRE), North Myrtle Beach, SC -
United States of America
|
| Phase: | Landing |
| Nature: | Private |
| Departure airport: | Hendersonville Airport, NC (0A7) |
| Destination airport: | Myrtle Beach-Grand Strand Airport, SC (CRE/KCRE) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that during a cross-country flight in night, visual meteorological conditions, the airplane’s alternator failed. He described that he misinterpreted the alternator warning light illuminating, and did not realize that the alternator had failed. Some time later the battery failed, resulting in a total loss of electrical power. He recalled making the decision to continue to his originally intended destination because of his familiarity with the airport. As he entered the downwind leg of the traffic pattern at the destination airport, he began his emergency checklists in preparation for landing. While performing the checklists he noticed that the airplane’s speed was too fast, so he attempted to extend the flaps to slow down. Upon activation, he realized they would not function without electrical power. Amid these efforts he continued the emergency checklist, pulling what he thought was the hydraulic system circuit breaker, but what a post-accident inspection revealed to actually be the standby vacuum pump circuit breaker. The pilot reported that he continued setting up the airplane for landing but did extend the landing gear using the emergency gear extension system. The pilot subsequently landed the airplane with the landing gear still up, resulting in substantial damage to the fuselage’s external longerons.
A postaccident examination of the airplane revealed that the emergency landing gear extension handle was in the stowed position. The emergency landing gear extension system was functionally tested while the airplane was on jacks and found to function satisfactorily. Once electrical power was restored, the landing gear retraction/extension system operated normally. Additionally, the alternator belt was found broken, which likely resulted in the alternator’s failure during the flight.
Probable Cause: The pilot’s failure to use the emergency landing gear extension system, resulting in a gear-up landing. Contributing to the accident was an alternator belt failure.
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | |
| Status: | Investigation completed |
| Duration: | 1 month |
| Download report: | Final report
|
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Sources:
NTSB
https://data.ntsb.gov/Docket?ProjectID=194838 Location
Images:

Photo: NTSB
Revision history:
| Date/time | Contributor | Updates |
| 31-Jul-2024 05:35 |
ASN |
Added |
| 31-Jul-2024 06:07 |
ASN |
Updated [Location, ] |
| 13-Aug-2024 07:26 |
Captain Adam |
Updated [Time, Location, Nature, Departure airport, Source, Damage, Category, Accident report, ] |
| 12-Sep-2024 11:59 |
Captain Adam |
Updated [Source, Narrative, Photo, ] |
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