| Date: | Saturday 16 June 1990 |
| Time: | 15:30 |
| Type: | Rutan VariEze |
| Owner/operator: | private |
| Registration: | N3KJ |
| MSN: | 848 |
| Engine model: | Lycoming O-235 C2C |
| Fatalities: | Fatalities: 1 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Destroyed |
| Category: | Accident |
| Location: | Brainard, NE -
United States of America
|
| Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
| Nature: | Private |
| Departure airport: | Omaha, NE (MLE) |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AFTER MAKING A LOW, HIGH SPEED PASS, OVER A PRIVATE AIRSTRIP, THE HOMEBUILT ACFT WAS OBSERVED TO PULL UP, ROLL TO THE LEFT ABOUT 180 DEGREES TO AN INVERTED ATTITUDE, THEN DESCEND ALMOST VERTICALLY TO THE TERRAIN. NO MECHANICAL MALFUNCTIONS OR DEFECTS WERE DISCOVERED IN THE POST ACCIDENT INVESTIGATION. CAUSE: PILOT USED POOR JUDGEMENT IN ATTEMPTING AEROBATICS WITH INADEQUATE ALTITUDE WHICH RESULTED IN LOSS OF AIRCRAFT CONTROL. CONTRIBUTING FACTORS WERE A LOW PASS PERFORMED, OVER CONFIDENCE IN PERSONAL ABILITY AND OSTENTATIOUS DISPLAY BY THE PIC.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | MKC90DCJ01 |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
|
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001212X23487 Revision history:
| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
| 21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency, ] |
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