Accident Midget Mustang N76JF,
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ASN Wikibase Occurrence # 41020
 
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Date:Monday 29 June 1998
Time:20:00 LT
Type:Silhouette image of generic MIMU model; specific model in this crash may look slightly different    
Midget Mustang
Owner/operator:David Lee Cruse
Registration: N76JF
MSN: 786
Total airframe hrs:253 hours
Engine model:Lycoming O-320-A3B
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Tracy, CA -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:(KTCY)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The experimental airplane was on climbout following a touch-and-go landing. During the climb, the engine began sputtering and lost power. The airplane leveled off momentarily and then began a steep left turn back toward the runway. During the turn, the airplane descended and collided with a power line. The engine had lost power in flight on several prior occasions. The airplane was not equipped with a fuel boost pump or an engine-driven fuel pump. The fuel tank was mounted in the fuselage, immediately forward of the instrument panel with no accumulator tank. The headspace between the fuel tank and the carburetor was reduced whenever the airplane's pitch attitude increased. A minimum of 0.5 pounds of fuel pressure at the carburetor inlet is required for operation of the engine. The minimum flow volume required for engine operation is not specified. The tank had a single, under wing vent line. Dirt and a piece of plastic were found lodged in the 90-degree elbow of the fuel tank vent line at the point where the line enters the tank. The dirt had formed a ball and was located on the tank side of the piece of plastic. The fuel tank was also equipped with a vented fuel cap that was found in place; however, the vent hole in the cap had been covered with gray silicon sealant.

Probable Cause: inadequate maintenance/inspection by the owner/pilot that resulted in an obstructed fuel vent system and a subsequent loss of engine power during takeoff.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX98FA208
Status: Investigation completed
Duration: 1 year and 11 months
Download report: Final report

Sources:

NTSB LAX98FA208

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Apr-2024 09:50 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report]

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