| Date: | Saturday 18 April 1998 |
| Time: | 21:30 LT |
| Type: | Quickie Q2 |
| Owner/operator: | D.t. Foster & D.l. Hilsman |
| Registration: | N996DT |
| MSN: | 2365 |
| Total airframe hrs: | 86 hours |
| Engine model: | Revmaster 2100-D |
| Fatalities: | Fatalities: 2 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Destroyed |
| Category: | Accident |
| Location: | Siloam Springs , AR -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | (KSLG) |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The amateur-built experimental Quickie airplane, occupied by a commercial pilot and a pilot-rated passenger, who were the co-owners/builders of the airplane, impacted the ground in a steep left bank during a forced landing following a partial loss of engine power. Disassembly of the engine revealed that six cylinder head hold-down nuts were loose, and combustion gases had been leaking between the cylinder heads and the barrels of the #2, #3, and #4 cylinders. The escaping gases cut a passage about 3/4 inch in diameter through the #4 cylinder head, resulting in the partial loss of engine power. Maintenance records indicated new cylinder heads were installed 33 hours before the accident in May 1997. A condition inspection of the airplane, which would have included a cylinder compression check, was due in November 1997, but had not been performed. According to a family member, the two owners were in the process of performing a condition inspection on the day of the accident; however, neither owner held a repairman certificate for the airplane or was a certificated airframe and powerplant mechanic.
Probable Cause: The pilot's failure to maintain aircraft control during the forced landing. Factors were the failure of the #4 cylinder head which resulted in a partial loss of engine power and the co-owners/builders' failure to perform a condition inspection of the airplane, which would have detected the leaking cylinder heads prior to the failure of the #4 cylinder head.
Accident investigation:
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| Investigating agency: | NTSB |
| Report number: | FTW98FA186 |
| Status: | Investigation completed |
| Duration: | 2 years and 6 months |
| Download report: | Final report
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Sources:
NTSB FTW98FA186
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
| 21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency, ] |
| 07-Apr-2024 13:41 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Source, Narrative, Category, Accident report, ] |
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