Accident Beechcraft 23 Muskeeter N2376L, Wednesday 7 August 2024
ASN logo
 

Date:Wednesday 7 August 2024
Time:15:44
Type:Silhouette image of generic BE23 model; specific model in this crash may look slightly different    
Beechcraft 23 Muskeeter
Owner/operator:Private
Registration: N2376L
MSN: M-212
Year of manufacture:1963
Fatalities:Fatalities: 0 / Occupants: 2
Other fatalities:0
Aircraft damage: Substantial
Category:Accident
Location:Herlong Recreational Airport (HEG/KHEG), Jacksonville, FL -   United States of America
Phase: Landing
Nature:Private
Departure airport:Jacksonville-Herlong Airport, FL (KHEG)
Destination airport:Jacksonville-Herlong Airport, FL (KHEG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On August 7, 2024, at 1544 eastern daylight time, a Beech 23, N2376L, was substantially damaged when it was involved in an accident near Jacksonville, Florida. The private pilot and pilot-rated passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that the purpose of the flight was to fly in the traffic pattern to see if the engine was leaking oil, as he had recently observed trace amounts of oil in the cowling. After completing a normal preflight inspection and an engine run-up the pilot took off and completed one traffic pattern circuit overflying the runway. He climbed back to traffic pattern altitude and made an approach to the runway with the intent to land. The pilot reported that the airplane seemed slow as he approached the runway numbers, so he increased the throttle; however, the engine rpm decreased to near idle. He continued to report that, about 20 ft above ground level, the airplane dropped to the runway and landed hard on the runway centerline. The left main landing gear separated and the airplane skidded to a stop in the grass to the left of the runway. The left wing and fuselage received substantial damage.

A postaccident examination of the airplane and engine, which included a successful test run of the engine, did not reveal evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation. Following the accident, the fuel selector was found selected to the intact right wing fuel tank, which contained about 3 gallons of fuel. The left wing fuel tank contained about 9 gallons of fuel. According to the pilot operating handbook for the accident airplane, each fuel tank contained 3.8 gallons of unusable fuel. Based on this information, it is likely that the total loss of engine power was the result of fuel starvation.

Probable Cause: The pilot’s improper inflight fuel management, which resulted in a total loss of engine power due to fuel starvation while on final approach to land, and the subsequent hard landing, which resulted in separation of the airplane’s landing gear.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA24LA341
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB
https://data.ntsb.gov/Docket?ProjectID=194868

Location

Images:


Photo: NTSB

Revision history:

Date/timeContributorUpdates
20-Aug-2024 18:43 Captain Adam Added
11-Apr-2025 22:22 Captain Adam Updated [Source, Narrative, Photo, ]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2025 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org