ASN Wikibase Occurrence # 41595
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Date: | Thursday 9 December 1999 |
Time: | 20:09 LT |
Type: | Cessna 310N |
Owner/operator: | James T. Wynja |
Registration: | N5038Q |
MSN: | 310N-0138 |
Total airframe hrs: | 5000 hours |
Engine model: | Continental IO-470-VO |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Danville-Vermilion County Airport, Danville, IL -
United States of America
|
Phase: | Initial climb |
Nature: | Training |
Departure airport: | (KDNV) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The instructional flight crashed 1-sm mile south of the airport during initial climb. A witness reported that while the airplane was taking off he heard a, '...whoosh sound and thought an engine failure had occurred...' The witness stated that the aircraft, from an altitude of 100-200 feet above ground level (agl), started a high rate descent towards the runway, then recovered into level flight for a few seconds, then began a climb that took the aircraft into the clouds. Weather conditions at the time of the accident were reported to be instrument meteorological conditions with 2-sm visibility, partial obscuration due to light precipitation, and an overcast ceiling of 1,300-feet. The accident occurred during a dark night. The governing FAA air traffic control center, Champaign approach, reported no communications were received from or transmitted to the accident airplane and additionally no flight plan information was filed or requested. No anomalies were found with the airframe, or its related systems, that could be associated with a preexisting condition. No anomalies were found with either engine, or their related systems, that could be associated with a preexisting condition.
Probable Cause: Aircraft control not being maintained by the flight instructor and the flight instructor's inadequate supervision of the flight. Factors to the accident were the flight instructor's VFR flight into IMC weather conditions, the inadequate preflight planning/preparation conducted by the flight instructor, the dark night, the low ceiling, and the rain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI00FA039 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB CHI00FA039
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
30-Jun-2013 13:34 |
JINX |
Updated [Time, Operator, Location, Departure airport, Source] |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Dec-2017 09:59 |
ASN Update Bot |
Updated [Departure airport, Destination airport, Source, Narrative] |
07-Apr-2024 16:26 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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