ASN Wikibase Occurrence # 41820
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Date: | Wednesday 22 March 2000 |
Time: | 18:20 |
Type: | Cessna 177RG Cardinal RG |
Owner/operator: | Aircraft Holding Co. Llc |
Registration: | N1556H |
MSN: | 177RG0730 |
Total airframe hrs: | 1623 hours |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Columbia, SC -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | CUB |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative: According to the PIC, substantiated by the widow of the passenger/pilot, the airplane fuel tanks were topped off at Orangeburg Municipal Airport, Orangeburg, South Carolina, on March 19, 2000. The PIC further stated that he flew directly home to Columbia Downtown Airport, parked, and tied down for a total fuel burn time of about 30 minutes. On March 22, 2000, the airplane took off from Columbia Downtown Airport, the PIC having radioed his intention to stay in the traffic pattern, and sustained an engine stoppage as the airplane approached the abeam position for its first landing. The airplane collided with the terrain and revealed no evidence of onboard fuel at the crash site. The engine underwent a factory test cell run, and it was unsatisfactory until factory fuel injector nozzles were substituted, at which time the engine met factory specifications. Subsequent disassembly examination of the fuel system components revealed contamination in the fuel injector servo. The fuel quantity indication system underwent factory testing and revealed the right tank system was operating erratically, which appeared to be a precrash condition.
Probable Cause: The PIC's inadequate planning and preparation resulting in refueling not being performed and the subsequent fuel exhaustion and forced landing into trees. A factor in the accident was the erratic operation of the right fuel tank quantity indicating system.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA00FA117 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001212X20688&key=1 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Dec-2017 18:31 |
ASN Update Bot |
Updated [Operator, Departure airport, Source, Narrative] |
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