| Date: | Sunday 6 June 1999 |
| Time: | 23:16 LT |
| Type: | Boeing 747-4F6B |
| Owner/operator: | Philippine Airlines |
| Registration: | N751PR |
| MSN: | 27261/1005 |
| Year of manufacture: | 1993 |
| Total airframe hrs: | 66851 hours |
| Engine model: | GE CF6-80C2B1F |
| Fatalities: | Fatalities: 0 / Occupants: 425 |
| Other fatalities: | 0 |
| Aircraft damage: | Minor, repaired |
| Category: | Accident |
| Location: | Los Angeles International Airport, CA (LAX/KLAX) -
United States of America
|
| Phase: | Taxi |
| Nature: | Passenger - Scheduled |
| Departure airport: | Los Angeles International Airport, CA (LAX/KLAX) |
| Destination airport: | Manila International Airport (MNL) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Boeing 747-4F6B, N751PR, collided on the ground with a Boeing 747 SP-44, F-GTOM, at the Los Angeles International Airport (LAX), California. When the collision occurred N751PR, operated by Philippine Airlines as flight 103, was taxiing for takeoff with an intended destination of Manila, Philippines. F-GTOM, operated by Corsair as flight 942, was parking following its arrival from Paris, France. Onboard the Philippine airplane were 4 flight deck crewmembers, 16 cabin attendants, and 405 passengers. None of the 425 occupants were injured.
Onboard the Corsair airplane were 4 flight deck crewmembers, 9 cabin attendants, and 261 passengers. None of the 274 occupants were injured.
Visual meteorological conditions prevailed during the nighttime collision that occurred as the Philippine airplane taxied for takeoff in a westerly direction on taxilane "C," and collided with the Corsair airplane, which had stopped in a northwesterly direction short of its assigned gate 101, at the Tom Bradley International Terminal (TBIT). The Philippine airplane received minor damage. Its right winglet was severed. The Corsair airplane's left wing was substantially damaged.
Probable Cause: Airport management's failure to ensure that its current operating procedure, which required the arriving airplane to power into the terminal gate, was being used. Also causal was (1) the ground service company's utilization of an outdated arrival procedure that directed the arriving airplane to stop short of the gate, thereby obstructing the taxilane; and (2) the ground service company's utilization of a nonstandard marshalling hand signal which was, accordingly, misinterpreted by the departing airplane's crew. A contributing factor was the departing airplane's first officer's misjudged evaluation of wing tip clearance.
Accident investigation:
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| Investigating agency: | NTSB |
| Report number: | LAX99FA218 |
| Status: | Investigation completed |
| Duration: | 4 years and 5 months |
| Download report: | Final report
|
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Sources:
NTSB LAX99FA218
Location
Revision history:
| Date/time | Contributor | Updates |
| 13-Sep-2024 16:01 |
ASN Update Bot |
Added |
| 13-Sep-2024 16:20 |
ASN |
Updated [Cn, Operator, Total occupants, Location, Nature, Departure airport, Destination airport, Damage, Narrative, ] |
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