Accident Beechcraft D95A Travel Air N4835J,
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ASN Wikibase Occurrence # 42808
 
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Date:Saturday 27 August 1994
Time:18:05 LT
Type:Silhouette image of generic BE95 model; specific model in this crash may look slightly different    
Beechcraft D95A Travel Air
Owner/operator:Diamond K. Aviation, Inc.
Registration: N4835J
MSN: TD-679
Total airframe hrs:3913 hours
Engine model:Lycoming IO-360-B1B
Fatalities:Fatalities: 1 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Oakdale, CA -   United States of America
Phase: Unknown
Nature:Training
Departure airport:
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THIS WAS THE STUDENT'S FIRST FLIGHT IN A MULTIENGINE FLIGHT TRAINING COURSE. AFTER 3 TAKEOFFS & LANDINGS AT THE AIRPORT, THE FLIGHT DEPARTED THE AREA, THEN RETURNED A FEW MINUTES LATER. WHEN THE CFI TRANSMITTED THEIR POSITION, A GROUND-BASED WITNESS (ALSO A MULTI-ENGINE CFI) HEARD THE SOUND OF A GEAR WARNING HORN IN THE BACKGROUND. THE WITNESS OPINED THAT THE FLIGHT WAS PRACTICING A SINGLE ENGINE APPROACH. THE WITNESS OBSERVED THE AIRCRAFT DESCEND TO ABOUT 30' AGL AS IT OVERFLEW THE APPROACH END OF THE RUNWAY, THEN ENTER A SHALLOW CLIMBOUT. BEFORE REACHING THE DEPARTURE END OF THE RUNWAY, THE AIRCRAFT ENTERED A LEFT BANK. THE BANK ANGLE GRADUALLY INCREASED UNTIL BECOMING VERTICAL, AND THE AIRCRAFT CRASHED INTO A FIELD NEXT TO THE AIRPORT. AN EXAM OF THE WRECKAGE REVEALED NO PREIMPACT MECHANICAL MALFUNCTION. THE LEFT & RIGHT FUEL TANK SELECTORS WERE FOUND IN THE 'OFF' & 'MAIN TANK' POSITIONS, RESPECTIVELY. THE LEFT PROPELLER APPEARED TO HAVE BEEN IN THE FEATHER POSITION, THE RIGHT PROPELLER WAS TWISTED & BENT. THE CFI HAD GIVEN ABOUT 8 HOURS TOTAL OF MULTIENGINE INSTRUCTION (TO ANOTHER STUDENT) DURING THE 2.5 WEEKS SINCE HAVING BEEN ISSUED A MULTIENGINE INSTRUCTOR PILOT CERTIFICATE.

Probable Cause: IMPROPER IN-FLIGHT PLANNING/DECISION BY THE FLIGHT INSTRUCTOR (CFI), AND THE CFI'S INADEQUATE SUPERVISION BY NOT ASSURING THAT THE MINIMUM CONTROL SPEED (VMC) WAS MAINTAINED. A FACTOR RELATED TO THE ACCIDENT WAS: THE CFI'S LACK OF EXPERIENCE IN MULTI-ENGINE INSTRUCTIONAL TRAINING.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX94LA340
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB LAX94LA340

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Apr-2024 19:36 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Source, Narrative, Category, Accident report]

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