Accident Hughes 500D (369D) N277SP,
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ASN Wikibase Occurrence # 43276
 
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Date:Saturday 19 June 1993
Time:05:10 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes 500D (369D)
Owner/operator:Skydance Operations, Inc.
Registration: N277SP
MSN: 290461D
Year of manufacture:1979
Engine model:Allison 250-C20B
Fatalities:Fatalities: 1 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Half Moon Bay, CA -   United States of America
Phase: Initial climb
Nature:Ferry/positioning
Departure airport:
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot departed his residence in the southern California area at 1030 on June 18th and flew commercially to Reno, Nevada. The pilot was to pick up the helicopter and ferry it to a movie filming location at the accident site, where it was to be used as a camera platform. The pilot arrived in Reno at 1300 hours and was informed that the helicopter was not at the airport and ground transportation would be sent to take him to the helicopter. The pilot waited in the airport terminal until 1630 hours for ground transportation to arrive. At 1745 hours the pilot departed in the accident helicopter and arrived at the filming site about 1850 hours. The actual filming started just after midnight on saturday morning and concluded at 0300 hours that morning. About 0410 hours the pilot was maneuvering the helicopter to depart the area when it collided with a power cable attached to an illuminated bank of high intensity lights mounted on top of a 125 foot tall telescoping tower used during the filming. The impact occurred on the same side of the tower as the two million candle power lights. The accident occurred about 17 hours after the pilot had departed his residence.

Probable Cause: the pilots failure to maintain an adequate clearance from the light tower and associated electrical power cables. Factors in the accident were; 1) pilot fatigue due to an excessively long duty day, and 2) glare from the lights which affected the pilot's ability to clearly see the obsturctions.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX93LA261
Status: Investigation completed
Duration: 1 year
Download report: Final report

Sources:

NTSB LAX93LA261

History of this aircraft

Other occurrences involving this aircraft
1 September 1983 N277SP Southwestern Public Service 0 Portales, NM sub

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
10-Apr-2024 13:09 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Source, Narrative, Category, Accident report]

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