Accident Mooney M20F N9180V,
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ASN Wikibase Occurrence # 43751
 
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Date:Sunday 8 July 2007
Time:16:02
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20F
Owner/operator:Private
Registration: N9180V
MSN: 690046
Year of manufacture:1969
Total airframe hrs:4163 hours
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 2 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Brooks, KY -   United States of America
Phase: Landing
Nature:Private
Departure airport:Harrisburg, IL (HSB)
Destination airport:Louisville, KY (07KY)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot of a Mooney M20F, with three passengers onboard, attempted to land on a 2,150-foot turf strip with trees at both ends. During the landing, the airplane touched down fast and the pilot aborted the landing. He then joined the traffic pattern for a second attempted landing. During the second landing, the airplane touched down 506 feet down the runway and the pilot aborted the landing again. A passenger could see the tops of the trees and then heard the engine increase in power. During this time the airplane was observed in a nose-high attitude. Moments later it impacted the ground in a nose-low attitude and tumbled before coming to rest. The investigation revealed that the airplane had landed at the wrong airport (the destination airport runway was 150 feet shorter, and also had trees at both ends of the runway), had been overweight prior to departing, and was most likely over its maximum allowable operating weight while landing. The investigation also revealed that a passenger seatbelt had not been secured properly. During the impact sequence, an attachment fitting had detached, releasing the occupant from their seat restraint.
Probable Cause: The pilot's failure to maintain aircraft control during the aborted landing. Contributing to the accident was the exceedance of the airplane's maximum gross weight, and the pilot's inadequate preflight planning.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC07FA159
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070718X00957&key=1

History of this aircraft

Other occurrences involving this aircraft
5 September 1997 N9217V Sundance Aviation 0 Gulf of California w/o

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
04-Dec-2017 18:48 ASN Update Bot Updated [Cn, Operator, Other fatalities, Destination airport, Source, Narrative]

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