ASN Wikibase Occurrence # 43768
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 1 June 2007 |
Time: | 08:25 |
Type: | Christen A-1 Husky |
Owner/operator: | United States Department of Agriculture |
Registration: | N9602R |
MSN: | 1119 |
Total airframe hrs: | 6869 hours |
Engine model: | Textron Lycoming O-360-C1G |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Loa, UT -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Unknown |
Departure airport: | Richfield Muni, UT (RIF) |
Destination airport: | Loa, UT |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and gunner were participating in a low-level, aerial predatory control operation. They were operating over terrain that was approximately 8,300 feet above mean sea level. While maneuvering in a turn at slow airspeed to make an additional pass over an area with coyotes, the airplane impacted the ground with the right wing tip, and then came to rest inverted. A witness, who was working with the pilot from the ground, was in a drainage wash while the airplane circled overhead. They had just identified a coyote den and there were coyotes traversing up and down the wash. The airplane went out of the witness's view, and then the witness heard the impact of the airplane with the ground. No evidence of any preimpact mechanical anomalies was discovered. Weight and balance calculations showed that the airplane was out of its aft center of gravity limits by 1.6 inches, which would result in less stable flight characteristics, especially during slow flight. Previous accidents involving similar flight regimes have been associated with wake vortices encounters. Although it is possible that the airplane encountered its own wake vortices, this could not be determined with the available evidence. Based on standard atmospheric conditions and the temperatures at the closest reporting stations, the density altitude would have been about 10,000 feet.
Probable Cause: The pilot's failure to maintain an adequate airspeed during low altitude maneuvering flight that resulted in a stall. The pilot's decision to operate the airplane at a center of gravity beyond the rear limit, the low altitude of the flight, and the high density altitude were contributing factors.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA07GA142 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070608X00696&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 18:43 |
ASN Update Bot |
Updated [Other fatalities, Nature, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation