ASN Wikibase Occurrence # 43870
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Date: | Friday 9 February 2007 |
Time: | 18:15 |
Type: | Beechcraft A36 Bonanza |
Owner/operator: | Blue Heron Aviation Sales Llc |
Registration: | N506BC |
MSN: | E-1024 |
Year of manufacture: | 1977 |
Total airframe hrs: | 3530 hours |
Fatalities: | Fatalities: 4 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hinesville , GA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Titusville, FL (TIX) |
Destination airport: | Anderson, SC (AND) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The instrument-rated private pilot filed an instrument-flight-rules flight plan and advised the controller that he was operating under visual-flight-rules flight at 9,500 feet. The controller cleared the pilot to descend and maintain 9,000 feet. Shortly thereafter, the pilot requested clearance to climb to 11,000 feet. The controller advised the pilot that there were reports of icing between 12,000 and 16,000 feet. The pilot advised that he would be "on top of it." The pilot requested clearance to climb to 13,000 feet. Shortly thereafter, the pilot advised he was "experiencing some precipitation" and requested clearance to descend to 11,000 feet. Analysis conducted by Safety Board meteorology specialists indicates that the airplane likely encountered freezing rain or drizzle that would have resulted in moderate to severe mixed icing adhering to its airframe. As the airplane descended in a right turn, it disappeared from radar. The airplane broke up in flight and impacted heavily wooded terrain. Marijuana was found at the scene, and post-accident toxicological testing performed on specimens from the pilot was consistent with the use of marijuana within 3 hours of the accident.
Probable Cause: The pilot's failure to maintain aircraft control resulting in the in-flight breakup of the airplane due to aerodynamic overload. Contributing to the accident were airframe icing and the pilot's impairment by illegal drugs.
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070215X00194&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 18:31 |
ASN Update Bot |
Updated [Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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