ASN Wikibase Occurrence # 44051
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Date: | Friday 4 August 2006 |
Time: | 10:30 |
Type: | Cessna A188B |
Owner/operator: | S&S Aviation |
Registration: | N86188 |
MSN: | 18802008T |
Year of manufacture: | 1975 |
Total airframe hrs: | 8030 hours |
Engine model: | Continental IO-520 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sumrall, MS -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Agricultural |
Departure airport: | Collins, MS |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The tail-wheel-equipped agricultural airplane stalled and impacted into a pond during a low altitude turn following a partial loss of engine power. The 1,525-hour commercial pilot had finished spraying a field and was departing the area when a witness observed the engine "pop as it would if the mixture was too lean." The engine then sounded as if it "cleared up" and moments later the airplane turned back towards the witness's location. As the airplane proceeded back towards him, the witness observed the engine running; however, it did not appear to be running at "full throttle." When the airplane was approximately 150-feet AGL, the airplane made a 90-degree turn before it "plunged" nose-first into a pond. All major components of the airplane were accounted for at the site, and control continuity was established to the airplane's flight controls. An examination of the engine revealed that the crankshaft, connecting rods and connecting rod bearings exhibited thermal and mechanical damage consistent with a lack of lubrication. The number four connecting rod bolt was found completely fractured. The oil sump, which had not been compromised during the accident, was found to contain residual oil. Investigators could not determine the reason for the loss of engine oil.
Probable Cause: The pilot's failure to maintain airspeed which resulted in an inadvertent stall. Contributing factors were the partial loss of engine power and the low altitude.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW06LA195 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20060807X01103&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
05-Dec-2017 09:20 |
ASN Update Bot |
Updated [Operator, Other fatalities, Source, Narrative] |
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