Accident Mooney M20C N6555U,
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ASN Wikibase Occurrence # 44404
 
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Date:Saturday 30 July 2005
Time:10:45
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20C
Owner/operator:Private
Registration: N6555U
MSN: 2338
Year of manufacture:1962
Total airframe hrs:3758 hours
Fatalities:Fatalities: 3 / Occupants: 4
Aircraft damage: Destroyed
Category:Accident
Location:Natchez, MS -   United States of America
Phase: Take off
Nature:Private
Departure airport:Natchez, MS (KHEZ)
Destination airport:Wichita Falls, TX (KT47)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane with the pilot and three passengers on board was departing for a cross country flight. A pilot witness was standing in front of the airport office building as the accident airplane was taking off on runway 31. He stated that the airplane "started a normal looking departure and climb out." However, "within a few hundred feet," he noticed the climb out was steeper than normal. The airplane started banking to the left while it continued to climb. The airplane "appeared to stall while still banking left," nosed down and impacted the ground. According to the surviving passenger, the takeoff roll was normal. Shortly after takeoff, it felt to her like the right wing and nose of the airplane were abruptly lifted up. She recalled that it was like someone pulled her backwards by her shoulders. At the same time, the pilot made a loud exclamation. She looked toward the pilot and could see through his side window that their height was just above the trees parallel to the runway. She also saw the ground, felt the airplane veer toward the left, and knew they were going to impact the ground. Examination of the wreckage at the accident site indicated the airplane impacted the ground in a left wing low and nose low attitude. No evidence was found of pre-impact mechanical discrepancies with the airframe or engine that would have prevented normal operation. According to his logbook, the pilot had accumulated about 126 hours total flight time of which 3.4 hours were in the accident airplane. No record of the pilot receiving any flight instruction from a certified flight instructor in the accident airplane or in any other complex airplane was found. In the endorsements section of the pilot's logbook, the endorsement required by 14 CFR Part 61.31(e), which certifies proficiency to operate a complex airplane, was blank.
Probable Cause: The pilot's failure to maintain adequate airspeed during the initial climb after takeoff, which resulted in an inadvertent stall and subsequent uncontrolled descent to ground impact. A contributing factor was the pilot's lack of experience in complex airplanes.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA05FA139
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20050805X01164&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
06-Dec-2017 10:41 ASN Update Bot Updated [Operator, Source, Narrative]

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