| Date: | Tuesday 8 October 2024 |
| Time: | 14:00 LT |
| Type: | Air Tractor AT-802A Fire Boss |
| Owner/operator: | Aero Spray Inc |
| Registration: | N212FB |
| MSN: | 802A-0368 |
| Year of manufacture: | 2010 |
| Total airframe hrs: | 1861 hours |
| Engine model: | Pratt & Whitney PT6-67F |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Inguadona, MN -
United States of America
|
| Phase: | Landing |
| Nature: | Fire fighting |
| Departure airport: | Brainerd/Crow Wing County Airport, MN (BRD/KBRD) |
| Destination airport: | Brainerd/Crow Wing County Airport, MN (BRD/KBRD) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot of the amphibious firefighting airplane departed from a land-based airport with a hard surface runway. The pilot reported that he was distracted during the initial climb by another airplane flying towards him on what looked like a low approach. According to the pilot this disrupted his callout flow, and he did not retract the landing gear. The flight was part of a training event, and the pilot was supposed to scoop water at a lake northwest of the scene of a mock fire. When he arrived at the intended lake another firefighting airplane had just scooped water and advised him to use a south to north scoop line. The pilot stated that he did his pre-scoop checklist, putting his hand on the landing gear lever and verbalizing “handle forward, four blue for the water,' as he was watching the other airplane. He said it did not register that the landing gear lever was aft and not forward or that there were four green lights instead of four blue. When the airplane landed it decelerated quickly and nosed over before settling upright, which resulted in substantial damage to the wings. The pilot egressed the airplane without incident and saw the floats had separated from the airplane and that the landing gear were extended. The pilot reported that there were no preaccident mechanical failures or malfunctions of the airplane that would have precluded normal operation.
Probable Cause: The pilot's failure to properly configure the landing gear on the amphibious airplane before a water landing.
Accident investigation:
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| Investigating agency: | NTSB |
| Report number: | CEN25LA008 |
| Status: | Investigation completed |
| Duration: | 3 months |
| Download report: | Final report
|
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Sources:
NTSB CEN25LA008
https://www.flightaware.com/live/flight/N212FB/history/20241008/1847Z/KBRD/L%2046.95923%20-94.06755 Location
Revision history:
| Date/time | Contributor | Updates |
| 09-Oct-2024 01:08 |
Geno |
Added |
| 09-Oct-2024 15:35 |
AgOps |
Updated [Time, Aircraft type, Registration, Cn, Operator, Nature, Departure airport, Source, Narrative, ] |
| 15-Oct-2024 19:13 |
Captain Adam |
Updated [Time, Location, Nature, Destination airport, Source, Damage, Narrative, Category, Accident report, ] |
| 25-Jan-2025 15:56 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Nature, Source, Narrative, ] |
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