ASN Wikibase Occurrence # 45482
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Date: | Thursday 25 July 2002 |
Time: | 12:59 |
Type: | Piper PA-30 Twin Comanche |
Owner/operator: | Private |
Registration: | N8563Y |
MSN: | 30-1679 |
Year of manufacture: | 1967 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Marble Hill, MO -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Sterling-Whiteside County Airport, IL (SQI/KSQI) |
Destination airport: | Newport, AR |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On July 25, 2002, at 1259 central daylight time, a Piper PA-30, N8563Y, owned and piloted by a private pilot, was destroyed when it impacted a 40 acre grass field near Marble Hill, Missouri. The pilot reported a loss of engine power and that he was landing in a field. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 personal flight was not operating on a flight plan. The pilot was fatally injured. The flight departed from the Whiteside County Airport, Rock Falls, Illinois, en route to Newport, Arkansas.
The airplane, owned and piloted by a private pilot, was destroyed during an off airport landing attempt. The pilot reported a loss of engine power while en route. Witnesses reported hearing engine noise when the airplane began to circle over a 40-acre grass field. The engine noise ceased about midpoint through the turn. Ground scarring and wreckage distribution was consistent with a nose down low-speed impact. Nonvolatile memory aboard the airplane showed that the left engine was colder than the right engine and that the pilot may have attempted to start the failed engine. Solid contamination of the fuel system was noted.
Probable Cause: The solid fuel system contamination resulting in a loss of engine power. The inadequate emergency procedures, and the airspeed not maintained by the pilot were additional causes.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20020805X01300&key=1 FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=8563Y
History of this aircraft
Other occurrences involving this aircraft
8 April 1978 |
N8563Y |
Sierra Corporation Inc |
0 |
Fairview Airport, Campobello, Landrum, South Carolina |
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sub |
Location
Images:
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2017 17:57 |
Dr.John Smith |
Updated [Time, Operator, Location, Departure airport, Destination airport, Source, Narrative] |
09-Apr-2017 18:01 |
Dr.John Smith |
Updated [Aircraft type] |
09-Dec-2017 16:56 |
ASN Update Bot |
Updated [Time, Operator, Departure airport, Destination airport, Source, Narrative] |
13-Sep-2023 13:16 |
Captain Adam |
Updated [[Time, Operator, Departure airport, Destination airport, Source, Narrative]] |
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