| Date: | Thursday 17 October 2024 |
| Time: | 15:30 LT |
| Type: | Cessna T206H Turbo Stationair HD |
| Owner/operator: | Trinity X Capital Holdings LLC |
| Registration: | N89S |
| MSN: | T20609524 |
| Year of manufacture: | 2017 |
| Total airframe hrs: | 492 hours |
| Engine model: | Lycoming TIO-540-AJ1A |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Tri-Cities Regional Airport (TRI/KTRI), Blountville, TN -
United States of America
|
| Phase: | Take off |
| Nature: | Private |
| Departure airport: | Blountville, TN |
| Destination airport: | Lexington-Blue Grass Airport, KY (LEX/KLEX) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that the airplane yawed left during takeoff and initial climb. At about 15 ft above ground level, he was unable to regain directional control and reduced engine power to land back onto the runway. The airplane landed left of the runway centerline, veered left, and then exited the left side of the runway. During the excursion, the nose and right main landing gear collapsed, and the right wing impacted the ground. The airplane came to rest in a grassy area adjacent to the runway. The airplane sustained substantial damage to its fuselage and right wing.
Post-accident examination of the airplane by a Federal Aviation Administration inspector revealed the rudder trim indicator was positioned to a partial nose left trim setting. Flight control continuity was established from the cockpit to all flight control surfaces. The examination revealed that there were no preaccident mechanical malfunctions or failures that would have precluded normal operation.
The pilot stated that additional right rudder input could have prevented the accident.
Probable Cause: The pilot's failure to maintain directional control during takeoff and subsequent rejected takeoff, which resulted in a runway excursion. Contributing to the accident was the pilot's failure to verify rudder trim setting prior to takeoff.
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | ERA25LA022 |
| Status: | Investigation completed |
| Duration: | 6 months |
| Download report: | Final report
|
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Sources:
NTSB ERA25LA022
FAA register:
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=89S Location
Revision history:
| Date/time | Contributor | Updates |
| 25-Oct-2024 11:12 |
Captain Adam |
Added |
| 24-Dec-2024 17:50 |
Captain Adam |
Updated [Time, Location, Departure airport, Destination airport, Category, Accident report, ] |
| 30-Apr-2025 11:47 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Source, Narrative, ] |
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