Gear-up landing Accident Beechcraft 58 Baron N458K, Friday 27 December 2024
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Date:Friday 27 December 2024
Time:18:30
Type:Silhouette image of generic BE58 model; specific model in this crash may look slightly different    
Beechcraft 58 Baron
Owner/operator:Kellair LLC
Registration: N458K
MSN: TH-452
Year of manufacture:1974
Fatalities:Fatalities: 0 / Occupants: 6
Other fatalities:0
Aircraft damage: Substantial
Category:Accident
Location:Florence Regional Airport (FLO/KFLO), Florence, SC -   United States of America
Phase: Landing
Nature:Private
Departure airport:Beckley Airport, WV (BKW/KBKW)
Destination airport:Florence Regional Airport, SC (FLO/KFLO)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was on a return, cross country flight to his home airport in instrument meteorological conditions. The pilot reported that he first performed a non-precision approach into the airport, where he reported that the landing gear extended normally. After performing a missed approach, the pilot retracted the landing gear and he then performed a precision approach in the opposite direction. The pilot reported that he put the landing gear switch in the down position, but that the landing gear did not extend. The pilot elected to continue the approach without troubleshooting, extending the gear manually, or referring to the emergency checklist. The pilot subsequently landed the airplane on the runway with the landing gear retracted, which resulted in substantial damage to the fuselage.

After the accident, the pilot performed an operational check and troubleshooting of the landing gear without authorization. The pilot reported that the landing gear again failed to extend, but would retract during his testing. The pilot also reported that the manual landing gear extension system operated normally. During the testing, the pilot said he found an “open circuit of the gear relay due to moisture or foreign debris.” After troubleshooting, the pilot reported that the landing gear started to operate normally. After the pilot had performed the unauthorized troubleshooting, a Federal Aviation Administration inspector examined the landing gear system, and performed a functional test, during which he found that it operated normally.

Probable Cause: The pilot’s failure to follow the emergency procedures and extend the landing gear manually after the landing gear did not initially extend normally.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA25LA094
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB
https://data.ntsb.gov/Docket?ProjectID=199523
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N458K
https://www.flightaware.com/live/flight/N458K/history/20241227/2230Z/KBKW/KFLO

https://photos.flightaware.com/photos/retriever/ca76e935f9168e18cb33fdb5259161e59651bc40 (photo)

Location

Revision history:

Date/timeContributorUpdates
30-Dec-2024 19:07 Captain Adam Added
22-Jan-2025 16:14 Captain Adam Updated [Time, Source, Accident report, ]
14-Jul-2025 02:35 Captain Adam Updated [Source, Narrative, ]

Corrections or additions? ... Edit this accident description

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