| Date: | Monday 19 May 1997 |
| Time: | 13:55 |
| Type: | Boeing 737-3Y0 |
| Owner/operator: | Monarch Airlines |
| Registration: | G-BWJA |
| MSN: | 24462/1691 |
| Year of manufacture: | 1989 |
| Engine model: | CFMI CFM56-3 |
| Fatalities: | Fatalities: 0 / Occupants: 56 |
| Other fatalities: | 0 |
| Aircraft damage: | Minor, repaired |
| Location: | London-Luton Airport (LTN/EGGW) -
United Kingdom
|
| Phase: | Take off |
| Nature: | Passenger - Scheduled |
| Departure airport: | London-Luton Airport (LTN/EGGW) |
| Destination airport: | Edinburgh-Turnhouse Airport (EDI/EGPH) |
| Investigating agency: | AAIB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The first officer was undergoing his first week of line training and had already completed 10 sectors, all under the supervision of the same Training Captain who was the commander on the incident flight; following satisfactory progress, the 'screen' first officer had been released after 8 sectors. The commander had assessed the previous 7 take offs, carried out by the first officer, as satisfactory. This flight was the first of the day for the crew. The weather was reasonable with light rain and a surface wind of 180°/08 kt; Runway 08 was in use.
Flap 1 was used for take off and the passengers were distributed evenly throughout the cabin. The ground roll was normal and thefirst officer commenced rotation at the commander's call of "Rotate";this had been calculated as 126 kt and was coincident with V1. The commander assessed that the aircraft nose pitched up more rapidly than normal but not excessively so and he considered it as a result of the light take-off weight. Subsequently, the climb was normal and the handling pilot leveled the aircraft at cruise flight level. However, one of the cabin attendants who had been seated at the rear of the aircraft had noted an unusual noiseat take off and, during the cruise, reported the fact to the commander. There had been no comment from ATC at Luton and a check of the cockpit indications revealed no adverse indications; the pressurization had performed normally during the
climb and level off. Therefore, the commander decided to continue the flight to Edinburgh and the
first officer made a normal landing at 1442 hrs.
After arrival on the stand, the commander checked the rear of the aircraft and noted that the water drain mast had scrape marks. He postulated that this had occurred on take off from Luton and informed the aircraft ground engineers. Checks of the airframe confirmed the scrape marks on the drain mast but no other damage.
Accident investigation:
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|
| | |
| Investigating agency: | AAIB |
| Report number: | |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
|
Sources:
https://assets.publishing.service.gov.uk/media/5422ee1bed915d13710001c9/dft_avsafety_pdf_500586.pdf https://www.jetphotos.com/photo/125571 (Photo)
Revision history:
| Date/time | Contributor | Updates |
| 01-Apr-2025 18:55 |
Justanormalperson |
Added |
| 01-Apr-2025 18:56 |
ASN |
Updated [Narrative, Accident report, ] |
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