| Date: | Tuesday 1 October 1996 |
| Time: | 23:21 UTC |
| Type: | McDonnell Douglas MD-83 |
| Owner/operator: | Sunways Intersun |
| Registration: | TC-INC |
| MSN: | 49792/1655 |
| Year of manufacture: | 1989 |
| Engine model: | P&W JT8D-200 |
| Fatalities: | Fatalities: 0 / Occupants: 144 |
| Other fatalities: | 0 |
| Aircraft damage: | Minor |
| Category: | Incident |
| Location: | Kajaani Airport (KAJ/EFKI) -
Finland
|
| Phase: | Take off |
| Nature: | Passenger - Non-Scheduled/charter/Air Taxi |
| Departure airport: | Kajaani Airport (KAJ/EFKI) |
| Destination airport: | Dalaman Airport (DLM/LTBS) |
| Investigating agency: | AIB Finland |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On Monday September 30, 1996 an aircraft left engine damage took place during flight SWW 2721 from Dalaman, Turkey to Cologne/Bonn, Germany with a Douglas DC-9-83 (MD-83) aircraft, registered TC-INC, owned by Irish Aerospace Finance Ltd and oper-ated by Turkish Intersun Sunways Havacilic A.S. A loud bang was heard in the cockpit from the left engine two to three minutes after reaching the cruising flight level. The engine continued to run but with increased Exhaus Gas Temperature (EGT), high pressure compressor rotation speed (N2) and fuel flow. The aircraft landed in Cologne/Bonn as planned. There were 129 passengers and seven crew members on board.
No qualified trouble shooting was performed in Cologne/Bonn and flight SWW 2722 departed for Kajaani, Finland with seven crew members on board but without passengers as planned. In the beginning of the takeoff the difference between the left and the right engine acceleration rates to 1,4 Engine Pressure Ratio (EPR) had increased significantly compared to the previous takeoff in Dalaman with the left engine being slower. During the flight to Kajaani the left engine surged when thrust was reduced from climb to cruise first at Flight Level (FL) 350 and later on at FL 330.
The serviceability of the left engine was not assured in Kajaani. A total of 137 passen-gers boarded the aircraft and the crew prepared for the flight SWW 2042 to Dalaman. The aircraft taxied out to the runway and the cockpit crew performed the normal procedures prior to takeoff. A loud banging noise was heard in the aircraft and at the terminal building when thrust was increased and the aircraft made a 180 turn into takeoff position. When the throttles were advanced for takeoff, the left engine did not accelerate normally. The left engine EGT was fluctuating with high peaks and the loud ban ing noise was heard again. The cockpit crew waited for approximately 40 s for the left engine to accelerate. When the engine did not accelerate, takeoff was aborted.
Accident investigation:
|
|
| | |
| Investigating agency: | AIB Finland |
| Report number: | |
| Status: | Investigation completed |
| Duration: | 1 year and 5 months |
| Download report: | Final report
|
|
Sources:
https://turvallisuustutkinta.fi/material/attachments/otkes/tutkintaselostukset/en/ilmailuonnettomuuksientutkinta/1996/b111996l_tutkintaselostus/b111996l_tutkintaselostus.pdf https://www.jetphotos.com/photo/5732466 (Photo)
History of this aircraft
Other occurrences involving this aircraft
| 11 April 1997 |
TC-INC |
Sunways Intersun |
0 |
Joensuu Airport (JOE/EFJO) |
 |
non |
| Runway excursion |
Revision history:
| Date/time | Contributor | Updates |
| 19-Jun-2025 16:14 |
Justanormalperson |
Added |
| 19-Jun-2025 16:15 |
Justanormalperson |
Updated [Accident report, ] |
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