ASN Wikibase Occurrence # 58470
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Date: | Sunday 11 January 2009 |
Time: | 21:16 |
Type: | Piper PA-46-500TP Malibu Meridian |
Owner/operator: | Private |
Registration: | N428DC |
MSN: | 4697124 |
Year of manufacture: | 2002 |
Engine model: | Pratt & Whitney Canada PT6A-42A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | East Milton, Florida -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Anderson, IN (AID) |
Destination airport: | Destin, FL (DTS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot filed a flight plan from his home airport to an airport about 1 mile from the Gulf of Mexico. During the flight, the pilot reported to air traffic control that he was encountering moderate to severe turbulence and, later, that the windshield was "cracking." After reporting the loss of the airplane’s door, the pilot advised that the windshield "has gone." The pilot later transmitted that the airplane’s flight controls were locked, that he was bleeding profusely, and that he was "graying out." The pilot further advised that he intended to "point the aircraft at the gulf," and he then parachuted from the airplane without advising air traffic control. As the airplane continued toward the Gulf of Mexico, air traffic controllers continued attempts to assist the pilot, with no response. The airplane eventually impacted wooded terrain, under power, about 18 nautical miles north of the Gulf of Mexico and about 100 yards from a residential area. An examination of the wreckage revealed no preimpact failures or malfunctions, that the door was still attached to the airframe, and that the windshield was undamaged and secured in its frame. A law enforcement investigation subsequently determined that the pilot, who was facing legal problems, intentionally parachuted from the aircraft near where he had previously stashed a motorcycle. The pilot was apprehended and subsequently plead guilty to federal criminal charges.
Probable Cause: The pilot's intentional inflight abandonment of the airplane.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09FA133 |
Status: | Investigation completed |
Duration: | 1 year and 11 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
12-Jan-2009 06:11 |
robbreid |
Added |
12-Jan-2009 06:12 |
harro |
Updated |
12-Jan-2009 09:58 |
gunther.kenya |
Updated |
06-Jun-2009 01:45 |
slowkid |
Updated |
16-Sep-2010 15:14 |
harro |
Updated [Source] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 11:39 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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