ASN Wikibase Occurrence # 58593
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Date: | Friday 30 January 2009 |
Time: | 08:10 |
Type: | Cessna 421C |
Owner/operator: | Fly High Inc |
Registration: | N345JB |
MSN: | 421C0494 |
Total airframe hrs: | 8034 hours |
Engine model: | Continental GTSIO-520-L |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | NE of Wichita, KS -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Wichita, KS (AAO) |
Destination airport: | Omaha, NE (MLE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During initial climb, the air transport pilot reported a loss of engine power. Unable to return to a runway, the pilot elected to perform a gear-up forced landing to an open field. The twin-engine airplane was substantially damaged during the landing. A line person employed by the fixed base operator (FBO) incorrectly fueled the airplane with 80 gallons of Jet-A instead of 100LL. Two medium single-engine general aviation airplanes based at the FBO had been modified with turbo-prop engines requiring Jet-A fuel. The two modified airplanes were not required by Supplement Type Certificate to modify the fuel filler opening, allowing the airplane to operate with smaller fuel filler openings,which did not comply with certification regulations. Line personnel at the FBO discovered that by rotating the Jet-A nozzle and dispensing at a reduced pressure, Jet-A fuel could be dispensed without using the adapter. Despite having correctly fueled the accident airplane in the past, the line person mistook the accident airplane for one of the converted airplanes and dispensed Jet-A fuel.
Probable Cause: The failure of line personnel to ensure that the airplane was serviced with the proper fuel. Contributing to the accident was the Federal Aviation Administration's approval of a Supplemental Type Certificate (STC) which allowed an improper fuel filler opening, and the complacency in non-standard fueling practices by fixed base operator (FBO) line personnel.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN09LA145 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/live/flight/N345JB/history/20090130/1410Z/KAAO/KMLE http://www.kake.com/home/headlines/38694527.html Location
Revision history:
Date/time | Contributor | Updates |
31-Jan-2009 11:12 |
harro |
Added |
28-Mar-2009 01:27 |
angels one five |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 11:39 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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