ASN Wikibase Occurrence # 59662
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Date: | Thursday 23 April 2009 |
Time: | 15:00 |
Type: | Piper PA-28R-200 Cherokee Arrow |
Owner/operator: | Private |
Registration: | N2938R |
MSN: | 28R-35333 |
Year of manufacture: | 1969 |
Total airframe hrs: | 3661 hours |
Engine model: | Lycoming IO-360-C1C |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hilliard, Florida -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Chattanooga, TN (1A0) |
Destination airport: | Winter Haven, FL (GIF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Approximately 2 hours into the cross-country flight the pilot heard a loud noise from the engine compartment and the engine subsequently failed. The pilot performed a forced landing in a field and the empennage struck a tree, resulting in substantial airframe damage. Examination of the engine revealed that the No. 3 cylinder partially separated in flight, resulting in the engine failure. An engine cylinder attachment stud and nut were found at the run-up pad at the departure airport. Examination of the stud revealed evidence of fatigue cracking, which was indicative of an under torque condition. Other cylinder attachment nuts on the engine showed evidence of under torquing. The pilot had recently purchased the airplane and the seller reported that an oil leak was noted during the "pre-buy" inspection. The mechanic who inspected the airplane at the pre-buy reported that two cylinders were leaking oil. The seller installed the cylinders as part of a major overhaul that occurred approximately 131 hours prior to the accident. The pilot did not have maintenance performed to address the cylinder oil leaks prior to the accident.
Probable Cause: A total loss of engine power due to the fatigue failure of the No. 3 cylinder attachment stud as a result of insufficient torque during installation. Contributing to the accident was the pilot’s operation of the airplane with a known mechanical deficiency.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09LA261 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
photo FAA
Revision history:
Date/time | Contributor | Updates |
23-Apr-2009 21:30 |
slowkid |
Added |
23-Apr-2009 21:36 |
slowkid |
Updated |
05-Mar-2010 10:45 |
harro |
Updated [Time, Departure airport, Source, Narrative] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 18:54 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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