Accident Beechcraft A36TC Bonanza C-FFIH,
ASN logo
ASN Wikibase Occurrence # 69457
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Tuesday 27 October 2009
Time:08:42
Type:Silhouette image of generic BT36 model; specific model in this crash may look slightly different    
Beechcraft A36TC Bonanza
Owner/operator:Private
Registration: C-FFIH
MSN: EA258
Year of manufacture:1981
Total airframe hrs:3167 hours
Engine model:Teledyne Continental TSIO-520-UB
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Near Kalamazoo/Battle Creek International Airport (KAZO), Michigan -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Kalamazoo, MI (AZO)
Destination airport:Muskoka, ON, (CYQA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Witnesses and global positioning system data indicated that after takeoff the airplane tracked the runway centerline and climbed approximately 150 feet above ground level before turning to the right and descending. The airplane subsequently impacted the ground, a fence, and a pole about 1,400 feet from the departure end of the runway. A postimpact fire ensued. After acknowledging the takeoff clearance, no further communications were received from the accident airplane. Examination of the airplane’s structure, flight controls, engine controls, and fuel system did not reveal any anomalies consistent with a preimpact failure. The engine manufacturer had issued a Mandatory Service Bulletin (MSB) that was applicable to the accident airplane’s engine. The airplane’s engine was disassembled in order to replace components damaged during the impact sequence. During the disassembly the valve lifters that were the subject of the MSB were examined and found to have pitting. However, the engine was reassembled with the original valve lifters for a functional test run and during the test run the engine produced full rated power and no anomalies were noted. Data retrieved from an engine monitoring system installed on the accident airplane recorded a significant reduction in engine power during the accident takeoff. The monitoring system did not record throttle, mixture, or propeller control positions and the data was consistent with normal power reductions recorded during the landing phase of previous flights. No mechanical reason for the loss of engine power was found.
Probable Cause: The loss of engine power for an undetermined reason.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: A09F0151
Status: Investigation completed
Duration: 1 year and 2 months
Download report: Final report

Sources:

NTSB

Location

Images:


Photo: NTSB

Revision history:

Date/timeContributorUpdates
27-Oct-2009 08:48 slowkid Added
27-Oct-2009 09:32 robbreid Updated
05-Oct-2010 15:34 Anon. Updated
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
02-Dec-2017 17:07 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org