ASN Wikibase Occurrence # 72365
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Date: | Thursday 4 February 2010 |
Time: | 15:00 |
Type: | Piper PA-32R-301T Saratoga II TC |
Owner/operator: | Private |
Registration: | N1060X |
MSN: | 3257466 |
Year of manufacture: | 2007 |
Total airframe hrs: | 319 hours |
Engine model: | Lycoming TIO-540-AH1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | 2 miles east of Stocktonhill Rd. at milepost 37.5, 20 miles n. of KIGM -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Saint George, UT (SGU) |
Destination airport: | Kingman, AZ (IGM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot/owner reported that about 30 minutes into the flight, he began to smell fuel. A short time later, the smell became stronger and was accompanied by a sensation of deceleration with no corresponding engine roughness. He immediately initiated an emergency descent and landed in a dry lake bed. During the landing flare, smoke began to stream from the front of the airplane, and after landing the fuselage was consumed by fire. Examination of the fuel inlet line which connects the fuel servo to the fuel flow divider revealed that it was approximately 1 1/2 turns loose at the 'B' nut fitting at the fuel flow divider. Fueling records indicated that at minimum, the airplane had flown 25 to 40 hours since the annual inspection, which was completed 5 months prior to the accident. The mechanic who performed the annual inspection specifically recalled verifying that the 'B' nut fitting was secure. The pilot reported that prior to the annual inspection the airplane had not been producing full power at takeoff. According to the pilot the deficiency was not resolved during the inspection, or on subsequent return trips to the maintenance facility. The pilot continued to fly the airplane with the discrepancy.
Probable Cause: The fuel flow divider inlet line nut coming loose during cruise flight, resulting in a fuel leak and in-flight fire. The root cause of the loose B-nut fitting could not be determined. Contributing to the accident was the pilot's decision to fly the airplane with a known deficiency.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10LA128 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
06-Feb-2010 02:07 |
RobertMB |
Added |
20-Jul-2010 11:02 |
harro |
Updated [Source] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 15:22 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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