ASN Wikibase Occurrence # 73423
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | 26-MAR-2006 |
Time: | 19:58 |
Type: | Airbus A321-211 |
Owner/operator: | My Travel Airways Scandinavia |
Registration: | OY-VKA |
MSN: | 1881 |
Fatalities: | Fatalities: 0 / Occupants: 223 |
Other fatalities: | 0 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Sandefjord Airport Torp (ENTO) -
Norway
|
Phase: | Landing |
Nature: | Passenger - Scheduled |
Departure airport: | Tenerife Airport (GCTS) |
Destination airport: | Sandefjord Airport Torp (ENTO) |
Investigating agency: | AIBN |
Confidence Rating: | Information verified through data from accident investigation authorities |
Narrative:An Airbus A321, registration OY-VKA and flight number VKG866, flew from Tenerife Airport (GCTS) to Sandefjord Airport Torp (ENTO) on 26th of March 2006.
The first officer was Pilot Flying (PF) and the commander was Pilot Not Flying (PNF). The crew reviewed updated weather and runway status before commencing the approach to ENTO. Air Traffic Information Services (ATIS) indicated dry runway and Braking Action (BA) GOOD.
When checking in on TWR frequency, the crew was informed that the runway was contaminated by 8 mm wet snow with a measured (Friction Coefficient, FC) of 32-33-31. These numbers indicated a MEDIUM BA.
The crew requested wind information in order to check for any crosswind or tailwind limitations. They made a mental consideration regarding the landing conditions and decided that it was acceptable to perform the landing. The airplane got high on the glide slope after passing 250 ft Radio Height. This resulted in a touch down approximately 780 metres from the threshold. After landing the crew experienced POOR braking action and suspected auto brake failure. The first officer performed maximum manual braking without noticing any BA. After landing the crew experienced POOR BA and suspected a brake failure. The commander took control, pulled the Park Brake (PB) and steered the aircraft with Nose Wheel Steering (NWS) towards the left side of the runway with guidance from the first officer.
The effect of the PB and NWS was that the aircraft skidded sideways towards the end of the runway 18. This resulted in increased deceleration and the aircraft stopped at the very end of the hard surfaced runway, with the nose wheel against a concrete antennae base.
The crew advised the TWR about the anticipated runway excursion while the aircraft skidded towards the end. This allowed the TWR to alert the fire and rescue crew even before the aircraft had stopped. The fire and rescue service functioned as expected.
No persons were injured and the aircraft got some skin and nose wheel damage. The commander shut down the engines and evacuated the passengers through the forward left cabin door. The passengers were transported to the terminal building by buses while the crew remained in the aircraft being towed to the terminal.
Sources:
https://www.aibn.no/Luftfart/Rapporter/2010-05-eng?pid=SHT-Report-ReportFile&attach=1
Accident investigation:
|
| |
Investigating agency: | AIBN |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Revision history:
Date/time | Contributor | Updates |
11-Mar-2010 11:02 |
harro |
Added |
13-Jan-2022 20:40 |
harro |
Updated [Narrative, Accident report] |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2023 Flight Safety Foundation