ASN Wikibase Occurrence # 75767
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 18 July 2010 |
Time: | 14:02 |
Type: | Beechcraft A36 Bonanza |
Owner/operator: | Reed Hatkoff |
Registration: | N9SH |
MSN: | E-981 |
Year of manufacture: | 1977 |
Total airframe hrs: | 3322 hours |
Engine model: | Lycoming Engines TIO-540-J2BD |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Deer Valley Road, close to Deer Valley Airport (KDVT), Phoenix, AZ -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Phoenix, AZ (DVT) |
Destination airport: | Phoenix, AZ (DVT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported flying for about an hour at 10,000 feet during a maintenance test flight to break in newly installed cylinders. The pilot reduced altitude to continue operating for another hour. As he changed altitude, he switched fuel tanks. Shortly after switching tanks, the engine lost power. During the forced landing, the airplane hit an automobile. Following the accident, about 1.5 gallons of fuel were recovered from the right fuel tank, and the left fuel tank was found empty. The right fuel tank was cracked and had leaked some fuel; the left fuel tank was not damaged. During the postaccident engine examination, no mechanical failures or malfunctions were revealed that would have precluded normal operation. The loss of engine power was most likely due to the pilot’s mismanagement of the fuel, resulting in fuel starvation.
Probable Cause: A loss of engine power during descent due to fuel starvation that resulted from the pilot's mismanagement of the fuel system.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10LA357 |
Status: | Investigation completed |
Duration: | 2 years 1 month |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
18-Jul-2010 21:17 |
Geno |
Added |
19-Jul-2010 02:01 |
RobertMB |
Updated [Time, Aircraft type, Operator, Location, Departure airport, Destination airport] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 17:59 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation