Accident Piper PA-46-350P Malibu Mirage N92358,
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ASN Wikibase Occurrence # 83475
 
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Date:Saturday 18 December 2010
Time:17:05
Type:Silhouette image of generic PA46 model; specific model in this crash may look slightly different    
Piper PA-46-350P Malibu Mirage
Owner/operator:Private
Registration: N92358
MSN: 4622147
Year of manufacture:1993
Total airframe hrs:1754 hours
Engine model:Lycoming TIO-540-AE2A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:NE of Lake Elmo Airport, Baytown Township MN -   United States of America
Phase: Approach
Nature:Private
Departure airport:Bowling Green, KY (BWG)
Destination airport:Anoka, MN (ANE)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
About an hour after takeoff the airplane was in cruise flight at 16,500 feet mean sea level (msl) when the pilot heard a loud noise followed by a rapid cabin depressurization. The pilot rapidly descended to 10,500 feet msl. The pressurization stabilized and he continued to his destination airport. About 3 hours and 25 minutes after takeoff, the airplane was approaching the destination airport and was about 1,500 feet above ground level when the engine suddenly lost power. The pilot attempted to restart the engine by putting the mixture, propeller, and throttle controls full forward. He turned on the emergency fuel pump and engaged the starter button, but the engine did not start. The pilot executed a forced landing at night to a field that had about 2 - 2.5 feet of snow in it. During the landing roll, the left wing separated from the fuselage. The inspection of the airplane revealed that the right wing fuel tank was empty. The left wing fuel tank was intact and appeared to be full of fuel. The fuel selector was found on the left tank. The pilot reported that he was certain that he had switched tanks sometime during the climb, but was not certain if he had switched tanks after that. The pilot reported that the loss of engine power was the result of fuel starvation.
Probable Cause: The pilot's improper fuel management which resulted in the loss of engine power due to fuel starvation. Contributing to the accident was the distraction of the cabin depressurization.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN11LA117
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB
https://flightaware.com/live/flight/N92358/history/20101218/1932Z/BWG341013/KANE

Location

Revision history:

Date/timeContributorUpdates
19-Dec-2010 10:37 bizjets101 Added
03-May-2014 14:26 Anon. Updated [Narrative]
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
26-Nov-2017 18:42 ASN Update Bot Updated [Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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