Accident Lancair IV-P N477RM,
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ASN Wikibase Occurrence # 134064
 
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Date:Tuesday 8 October 1996
Time:16:47 LT
Type:Silhouette image of generic LNC4 model; specific model in this crash may look slightly different    
Lancair IV-P
Owner/operator:Richards, Roger L.
Registration: N477RM
MSN: LIV-060
Total airframe hrs:12 hours
Engine model:Continental TSIO-550-B2B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Camarillo, CA -   United States of America
Phase: En route
Nature:Private
Departure airport:(KCMA)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The experimental airplane had been built from a kit by the pilot and flown about 12 flight hours since completion. Thirty-two gallons of fuel were onboard at the last takeoff, all of which was in the left tank. The engine lost total power at 4,500 feet msl with the fuel selector valve in the left tank position, and the pilot was unable to restart the engine. The engine was placed in a test cell with the fuel supply being routed to the engine through the aircraft's fuel selector valve. The engine started and developed only partial power. The No. 6 cylinder and piston exhibited heavy scorching, and after changing the cylinder and piston the engine operated to full power. The aircraft's fuel selector valve had been modified from the manufacturer's original configuration by machining to the valve's stem to incorporate a both position. The fuel selector was tested on a flow bench. Air bubbles were observed through the vapor ejector line when the line opposite the selected fuel tank was uncapped, simulating the empty right fuel tank. It was noted that as the air bubbles increased the fuel flow decreased from 253 lbs/hr to 235 lbs/hr. The engine requires 118 lbs/hr to operate at 75 percent power.

Probable Cause: The loss of engine power for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX97LA011
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB LAX97LA011

Location

Revision history:

Date/timeContributorUpdates
04-Jul-2012 00:53 harro Updated [Aircraft type, Operator, Narrative]
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
08-Apr-2024 18:34 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Source, Narrative, Category, Accident report]

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