ASN Wikibase Occurrence # 134953
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Date: | Tuesday 19 June 2007 |
Time: | 15:30 |
Type: | Mooney M20E |
Owner/operator: | C-NET Technologies |
Registration: | N115RC |
MSN: | 627 |
Year of manufacture: | 1965 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Van, TX -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Van, TX (5XS5) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The 1,010-hour commercial pilot lost control of the single-engine airplane while attempting to perform a short/soft field takeoff from a 2,000-foot grass airstrip that was oriented in a southwesterly direction. The pilot, who reported having accumulated a total of 184 hours in the same make and model, reported that right after liftoff from Runway 22, the airplane started to bank to the left. The pilot responded with a full right aileron application to slow the roll to no avail. An eye-witness at the airport reported observing the airplane "jump" off the ground after the nose of the airplane attained a pronounced nose-high attitude during rotation. The airplane struck the ground left wing first followed by the propeller and then the left side of the engine cowling. The pilot reported that he had gone to the airport to pick-up the airplane after airframe maintenance had been completed. The airplane had undergone repairs to the ailerons, flaps, rudder. flight instruments and avionics. The pilot that test flew the airplane prior to the release reported flying the airplane on 3 separate flights to make rigging adjustments. He added that all flight characteristics were normal. The FAA inspectors that responded to the accident site were able to establish flight control continuity. Additionally, they reported that based on the photos taken at the accident site, the elevator trim was in full-up position at the time of the accident. The airplane was not equipped with shoulder harnesses. The position of the wing flaps was not determined.
Probable Cause: The pilot's failure to maintain directional control during the takeoff run.
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070927X01459&key=1 Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 18:41 |
ASN Update Bot |
Updated [Operator, Departure airport, Destination airport, Source, Narrative] |
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