Wirestrike Accident Mooney M20E N3217F,
ASN logo
ASN Wikibase Occurrence # 135032
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Tuesday 23 May 2006
Time:18:30
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20E
Owner/operator:Bunk Aviation LLC
Registration: N3217F
MSN: 670010
Year of manufacture:1966
Total airframe hrs:3197 hours
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Blacksburg, SC -   United States of America
Phase: Take off
Nature:Private
Departure airport:Blacksburg, SC
Destination airport:Columbia, SC (KCUB)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated he was halfway down the runway when he observed the airspeed was 45 knots and he elected to continue the takeoff due to insufficient runway remaining to abort the takeoff. The commercial-rated passenger, the previous owner of the airplane, stated he observed the engine rpm decrease to 2400 rpm or less during the takeoff roll. Upon reaching the end of the runway the pilot stated he applied aft pressure on the control yoke and the airplane became airborne. The pilot retracted the landing gear, the airplane rolled right, and the nose pitched down. The pilot observed trees, power lines, and the airplane collided with the ground and a post crash fire ensued. A witness stated the pilot and two other personnel tried to turn the airplane around by hand before departure with negative results. The pilot entered the airplane, released the parking brake, exited the airplane, and the airplane was attempted to be moved again with negative results. The pilot and passenger entered the airplane and the pilot started the engine, turned the airplane around with power, and taxied to runway 06. The witness observed the airplane on its takeoff roll. The airplane traveled about 400 to 500 feet before reaching his location and the airplane ground speed was estimated at between 15 to 20 knots. The witness observed the airplane make an abrupt pitch up at the end of the runway and the tail down ring contacted the ground. The airplane became airborne rolled to the right, and disappeared from view. The runway was measured to be 1,383 feet long and 80 wide by the FAA. The Aircraft Owner's Manual showed the takeoff roll on a hard surface runway would be 790 feet, and 808 feet on a soft surface. Examination of the runway by the FAA revealed the airplane traveled 819 feet on the takeoff roll before encountering the dirt section of the runway. Two skid marks were present in the dirt on the runway. The left skid mark was measured 417 feet long and the right skid mark was measured 388 feet long. Ten feet past the left skid mark appeared to be a tail strike mark on a stone with a blue color. The bottom of the accident airplane is blue in color. Examination of the airplane revealed a post crash fire had destroyed the parking brake valve. The No.1 engine induction tube was damaged, separated from the No.1 cylinder intake port and both induction tube bolts were missing. One half of the No.1 intake gasket and one bolt with a locking star washer and a plain washer were located in the right side of the lower engine cowling. The bolt with locking star washer and plain washer was encased with molten aluminum, and the locking tabs on the washer were not flattened. A follow up examination by the FAA revealed thread damage was present on the No.1 cylinder induction tube bolt holes and improper sized threaded bolts had been installed in the No.1 and No. 3 cylinder induction tube bolt holes. Testing of an IO 360 engine at the engine manufacturer revealed with a separated induction tube from a cylinder intake port at 2,650 rpm, the engine rpm remained relatively constant. Engine rpm settings below 2,650 rpm revealed the engine would falter and rpm would decrease.









Probable Cause: The pilot's failure to abort the takeoff after the airplane failed to achieve adequate airspeed on the takeoff roll for undetermined reasons. This resulted in an abrupt pull up, inadvertent stall, and in flight collision with wires, trees and the ground.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL06LA083
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20060530X00640&key=1

Location

Revision history:

Date/timeContributorUpdates
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
05-Dec-2017 09:08 ASN Update Bot Updated [Operator, Departure airport, Destination airport, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org