ASN Wikibase Occurrence # 135221
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Date: | Monday 30 July 2007 |
Time: | 19:30 |
Type: | Netz KIS TR2 |
Owner/operator: | Private |
Registration: | N232AN |
MSN: | 115 |
Total airframe hrs: | 410 hours |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Willow Springs, MO -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Willow Springs, MO (1H5) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was destroyed when it impacted trees and terrain following a loss of control during flight. The pilot reported that he had performed a pre-flight examination of the airplane and no discrepancies were found. He said that after takeoff, he noticed that the airplane was flying left wing heavy. He said that he climbed to pattern altitude where he attempted a turn to the right. The right turn required more aileron input than was normal and the pilot decided to return to the airport. He said that he then made a left turn which became steep and he attempted to level the wings using right aileron at which time he felt something "let go." He was no longer able to control the airplane and it subsequently impacted trees and terrain. Examination of the airplane after the accident revealed that the left aileron push-pull control rod was separated into two pieces. Examination of the separated end fitting had portions of two rivets at 90 degrees to each other within the shank portion that inserts into the aluminum tube. The rivet shanks appeared to be machined or filed flush with the outside diameter of the insert. The aluminum pushrod tube had no evidence of drilled holes corresponding to the end fittings rivet locations, and no manufactured or shop formed rivet heads were present. No evidence could be found to indicate that the retaining rivets had been installed in the aluminum tube.
Probable Cause: The improper installation of the aileron control pushrod which led to a separation of the pushrod and subsequent loss of aircraft control. A factor was the pilot not being able to control the airplane after the pushrod separation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI07CA229 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070911X01368&key=1 Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 18:46 |
ASN Update Bot |
Updated [Departure airport, Source, Narrative, Plane category] |
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