Accident Christen Eagle II N88CE,
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ASN Wikibase Occurrence # 138372
 
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Date:Sunday 4 September 2011
Time:09:35
Type:Silhouette image of generic EAGL model; specific model in this crash may look slightly different    
Christen Eagle II
Owner/operator:Private
Registration: N88CE
MSN: LARSON-0001
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Near Seward, Nebraska -   United States of America
Phase: En route
Nature:Private
Departure airport:Seward, NE (SWT)
Destination airport:Seward, NE (SWT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight instructor, who was seated in the front seat, was giving the private pilot, who was seated in the rear seat, a check-out in the single-engine biplane. The engine lost power on takeoff, and the airplane impacted a field. Examination of the airplane and engine revealed no preimpact mechanical malfunctions or failures that would have precluded normal operation; however the mixture control lever, which was located below and to the left of the rear-seated pilot's left knee (there was no mixture control in the front seat), was pulled out about 2 inches. The lever should have been full forward during takeoff. The propeller control was situated directly below the mixture control and found in the full forward position. The propeller control lever is usually adjusted by the pilot after takeoff. Although the mixture and propeller control levers were color-coded, it's possible that the 6'5" private pilot's left knee blocked his view of the controls due to his size and the small cockpit. The mixture control knob was slightly larger than the propeller control knob, but both were similar in shape. It is possible that the pilot thought he was adjusting the propeller control rather than the mixture control on takeoff and inadvertently shut off fuel to the engine. Postaccident examination of the mixture control cable from the cockpit to the engine revealed it moved freely and there was no evidence it had been moved during impact.
Probable Cause: The pilot’s inadvertent pulling of the mixture control lever on takeoff, which shut down the engine.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN11FA616
Status: Investigation completed
Duration: 1 year and 8 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
05-Sep-2011 00:18 gerard57 Added
06-Sep-2011 08:54 gerard57 Updated [Aircraft type, Source, Narrative]
06-Sep-2011 11:09 RobertMB Updated [Aircraft type, Registration, Cn, Operator, Other fatalities, Departure airport, Narrative]
03-Dec-2017 16:10 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Damage, Narrative]

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