ASN Wikibase Occurrence # 143805
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Date: | Friday 17 February 2012 |
Time: | 12:07 |
Type: | Cessna 150J |
Owner/operator: | Private |
Registration: | N60276 |
MSN: | 15070190 |
Year of manufacture: | 1969 |
Total airframe hrs: | 3443 hours |
Engine model: | Continental O-200 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Pickens County Airport - KJZP, Jasper, GA -
United States of America
|
Phase: | Approach |
Nature: | Training |
Departure airport: | Jasper, GA (JZP) |
Destination airport: | Jasper, GA (JZP) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and the flight instructor reported that they conducted an extensive preflight inspection and filled the fuel tanks with fuel prior to departure for the pilot’s biennial flight review in the newly purchased airplane. They further reported that they sumped the fuel tanks before and after the refueling and noted no water or contamination. The takeoff was uneventful, and they remained in the traffic pattern to practice takeoffs and landings. While on final approach for the first landing, the pilot added power, and the engine subsequently sputtered and lost power. The flight instructor completed a forced landing to a field, and, during the landing roll, the airplane impacted a truck. Postaccident examination of the airplane and engine revealed large amounts of water in the fuel strainer bowl and carburetor bowl. Additionally, corrosion was observed inside the fuel tanks and the fuel strainer bowl, and the fuel cap gaskets appeared stiff and cracked. The airplane’s most recent annual inspection was completed about 6 months before the accident. The airplane had been stored outside while it was for sale, and it had only accumulated 4 hours of flight time in the previous 2 years and had not flown at all in the 3 months preceding the accident. Given the amount of water in the carburetor bowl and fuel strainer bowl, the poor condition of the fuel cap gaskets, and the presence of corrosion in the fuel tanks and fuel strainer bowl, it is likely that water had entered the fuel system during the time the airplane was stored outside. Further, it is unlikely that the pilots conducted a thorough preflight inspection, otherwise the water would have been detected.
Probable Cause: The pilots' inadequate preflight inspection that failed to detect water-contaminated fuel, which resulted in a total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA186 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
17-Feb-2012 13:11 |
RobertMB |
Added |
17-Feb-2012 15:34 |
Geno |
Updated [Location, Source] |
27-Feb-2012 16:08 |
Geno |
Updated [Time, Source, Narrative] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:19 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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