ASN Wikibase Occurrence # 144394
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Date: | Tuesday 13 March 2012 |
Time: | 09:50 |
Type: | Smith Aviation Super Cub |
Owner/operator: | Private |
Registration: | N712AZ |
MSN: | 04076 |
Year of manufacture: | 2008 |
Total airframe hrs: | 125 hours |
Engine model: | Mattituck TMX O-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | St. Johns Industrial Airpark - KSJN, St. Johns, AZ -
United States of America
|
Phase: | Landing |
Nature: | Ferry/positioning |
Departure airport: | St. Johns, AZ (SJN) |
Destination airport: | St. Johns, AZ (SJN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot had recently purchased the airplane and was receiving instruction in it. The pilot reported that the day before the accident, during landing, the left brake became less responsive than the right, and the airplane veered off of the runway but incurred no damage. The pilot and his flight instructor then bled the brake lines. This was followed by taxi and touch-and-go landing checks with no anomalies noted. The following morning the brakes were tested again and were operational. During the fourth landing that morning, the right brake locked up, and the airplane swerved to the right and nosed over. Although the flight instructor indicated that he had signed off the pilot for his tailwheel endorsement the day of the accident, he did not hold a current airman medical certificate. Additionally, the instructor reported that he did not remain on the flight controls with the pilot during the landings. Postaccident examination of the brake system revealed no evidence of a mechanical malfunction or failure that would have precluded normal operation.
Probable Cause: The pilots’ failure to maintain directional control when the right brake locked up during the landing roll for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR12LA135 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
https://www.faa.gov/data_research/accident_incident/preliminary_data/events01/media/02_712AZ.txt http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=712AZ&x=0&y=0 https://www.ntsb.gov/aviationquery/brief.aspx?ev_id=20120314X71745&key=1 https://www.flickr.com/photos/chrisk48/5118383994/_
History of this aircraft
Other occurrences involving this aircraft
31 January 2017 |
N712AZ |
Private |
0 |
Denton County, south of Northlake, TX |
|
sub |
Fuel starvation |
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2012 11:11 |
Geno |
Added |
22-Mar-2012 23:09 |
Geno |
Updated [Time, Nature, Departure airport, Source, Narrative] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:25 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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