ASN Wikibase Occurrence # 144933
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Date: | Tuesday 10 April 2012 |
Time: | 16:25 |
Type: | Piper PA-28-151 Cherokee Warrior |
Owner/operator: | Siherb Aviation Corp |
Registration: | N43003 |
MSN: | 28-7415407 |
Year of manufacture: | 1974 |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Off highway 25, halfway between Iuka and Tishomingo, MS -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Hammond, LA (HDC) |
Destination airport: | Franklin, IN (3FK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On the day before the accident, the pilot and passenger flew the airplane 575 miles from their home airport to conduct business. The pilot reported that during that flight he observed a discrepancy with the airplane's fuel quantity indicating gauges but that the gauges seemed to work correctly when he "pushed" on the edge of the instrument panel. After landing, the pilot requested that the airplane be refueled, but when he returned the next day to prepare for the return flight, the fuel tanks had not been filled. The pilot visually observed the fuel quantity in both fuel tanks and estimated that there was sufficient fuel for about 3.5 hours of flying, so he decided to take off and stop for fuel during the return flight. About 2.5 hours and 300 miles into the flight, the plot began searching for an airport where he could land and refuel the airplane. Shortly thereafter, the airplane's engine began losing power, so the pilot switched fuel tanks and diverted to nearest airport, which was about 14 miles away. About 4 miles from the airport, the engine lost all power, and the pilot performed a forced landing in a field. The airplane struck several trees during the landing roll, shearing the wings from the fuselage. The pilot reported no preimpact mechanical malfunctions or failures of the airplane, with the exception of the accuracy of the airplane's fuel gauges. Examination of the wreckage at the accident scene revealed no evidence of any fuel, fuel spillage, fuel leakage, or odor of fuel.
Probable Cause: The pilot's improper preflight planning and inflight fuel management, which resulted in a total loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12CA276 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
11-Apr-2012 05:07 |
gerard57 |
Added |
11-Apr-2012 05:57 |
RobertMB |
Updated [Time, Aircraft type, Registration, Operator, Location, Departure airport, Destination airport, Source, Narrative] |
11-Apr-2012 06:13 |
RobertMB |
Updated [Cn] |
11-Apr-2012 08:20 |
Geno |
Updated [Location, Narrative] |
11-Apr-2012 10:47 |
Anon. |
Updated [Location, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:35 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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