Accident Bellanca 17-30A Super Viking 300A N80SV,
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ASN Wikibase Occurrence # 145360
 
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Date:Friday 27 April 2012
Time:10:32
Type:Silhouette image of generic BL17 model; specific model in this crash may look slightly different    
Bellanca 17-30A Super Viking 300A
Owner/operator:Private
Registration: N80SV
MSN: 80-30971
Total airframe hrs:2575 hours
Engine model:Continental IO 520 SERIES
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Near runway 34, Cloverdale Municipal Airport - O60, Cloverdale, CA -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Cloverdale, CA (O60)
Destination airport:Palo Alto, CA (PAO)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that during the initial climb, about 2,000 feet above the ground, he switched to the auxiliary fuel tank and the engine lost power. He applied full throttle and mixture, as well as established a glideslope to return to the airport. The airplane descended faster than the pilot expected and impacted terrain short of the runway. A postaccident examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. The right, left, and auxiliary fuel tanks were all about a quarter full. The airplane flight manual states that the fuel selector valve should be on the main tank containing the most fuel during takeoff and landing. The auxiliary tank should only be used in level flight. During a climb, with the auxiliary fuel tank about one-quarter full, it is likely that fuel within the tank was insufficient to exit the tank through the fuel feed and therefore starved the engine of fuel.
Probable Cause: The pilot’s improper fuel management, which resulted in a loss of engine power during climb due to fuel starvation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR12LA185
Status: Investigation completed
Duration: 12 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
30-Apr-2012 19:17 Geno Added
08-May-2012 18:00 Geno Updated [Time, Location, Phase, Source, Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 20:37 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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