ASN Wikibase Occurrence # 146276
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Date: | Monday 11 June 2012 |
Time: | 07:40 |
Type: | Cessna 182A Skylane |
Owner/operator: | Private |
Registration: | N4715D |
MSN: | 34815 |
Year of manufacture: | 1957 |
Total airframe hrs: | 3813 hours |
Engine model: | Continental O-470 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | US Hwy 195, 5 miles north of Colfax, WA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Lewiston, ID (KLWS) |
Destination airport: | Spokane, WA (KSFF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Shortly after leveling off and beginning the cruise portion of the cross-country flight, the engine lost all power. The private pilot/owner performed a forced landing on a highway; however, just before the landing flare, the airplane’s vertical stabilizer struck a power cable and partially separated from the tailcone. Postaccident examination of the engine revealed that the carburetor drain plug was missing. The pilot stated that he had flown the airplane using automotive gasoline about 2 months before the accident. When the engine was subsequently difficult to start, the pilot removed the carburetor drain plug to purge the system of automotive fuel. He stated that he did not use safety wire to secure the plug after performing this operation.
Maintenance personnel examined the carburetor after the pilot reported that the engine was running rough (about 2 months before the accident) and again during the airplane’s annual inspection (about 1 month before the accident). Although maintenance personnel reported that on both occasions the drain plug was secured with safety wire, physical evidence suggested that the drain plug had never been secured with safety wire. Because of the contradictory statements and inconclusive evidence, it was not possible to determine who was responsible for the unsecured drain plug.
Probable Cause: The total loss of engine power during cruise flight due to the missing carburetor drain plug, which had not been secured with safety wire.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR12CA257 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
https://www.kxly.com/news/north-idaho-news/Plane-lands-on-highway-near-Colfax-clips-power-line/-/101230/14786308/-/c9ygiiz/-/index.html [LINK NOT WORKING ANYMORE:http://pullmanradio.com/viewNews.php?storyID=1134]
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=4715D&x=0&y=0 https://www.faa.gov/data_research/accident_incident/preliminary_data/events01/media/09_4715D.txt Location
Revision history:
Date/time | Contributor | Updates |
12-Jun-2012 22:41 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:46 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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