ASN Wikibase Occurrence # 157995
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Date: | Sunday 4 August 2013 |
Time: | 11:55 |
Type: | Beechcraft A36 Bonanza |
Owner/operator: | Aps Aviation Llc |
Registration: | N1831W |
MSN: | E-388 |
Year of manufacture: | 1973 |
Total airframe hrs: | 2778 hours |
Engine model: | Continental IO-550-B |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Near Alma, GA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Fernandia Beach, FL (FHB) |
Destination airport: | Lawrenceville, GA (LZU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was flying the airplane on a cross-country flight to his home airport in day visual meteorological conditions. While in cruise flight at 5,000 feet mean sea level (msl), the airplane began descending and was lost from radar at 2,800 feet msl, 2 miles from the accident site. The pilot did not transmit any distress calls to air traffic control. Witnesses near the accident site heard the airplane with the engine operating then shortly thereafter heard the sound of impact. Examination of the accident site indicated that the airplane had flown through trees at a shallow angle and impacted the ground on a road. Postaccident examination of the airframe and engine revealed no indications of preimpact anomalies; all observed damage was consistent with ground impact.
Postmortem examination of the pilot indicated that the cause of death was multiple blunt force injuries. The pilot's toxicology testing revealed medications that were unlikely to have contributed to the accident. Testing for carbon monoxide could not be performed due to unsuitable samples. A postmortem examination and toxicology tests were not performed on the passenger.
It could not be determined why the flight gradually descended from cruise altitude until impact with trees and the ground.
Probable Cause: Descent from cruise flight until impact with trees and the ground for reasons that could not be determined because postaccident examination of the wreckage did not reveal any anomalies that would have precluded normal operation and the pilot's autopsy and toxicology tests did not provide any evidence of impairment or incapacitation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA13FA349 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/live/flight/N1831W FAA register:
http://registry.faa.gov/AircraftInquiry/NNum_results.aspx?NNumbertxt=1831W Location
Revision history:
Date/time | Contributor | Updates |
04-Aug-2013 21:36 |
Geno |
Added |
06-Aug-2013 20:34 |
Geno |
Updated [Source] |
08-Aug-2013 21:59 |
Geno |
Updated [Time, Nature, Source, Damage, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 08:59 |
ASN Update Bot |
Updated [Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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