Accident Interstate S-1B1 Grasshopper N46336,
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ASN Wikibase Occurrence # 158657
 
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Date:Saturday 17 August 2013
Time:13:35
Type:Interstate S-1B1 Grasshopper
Owner/operator:Commemorative Air Force - Delaware Flying Wing
Registration: N46336
MSN: 159
Year of manufacture:1943
Total airframe hrs:892 hours
Engine model:Franklin 4ACG199H3
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Lancaster Airport (KLNS), Lancaster, PA -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Demo/Airshow/Display
Departure airport:Lititz, PA (LNS)
Destination airport:Lititz, PA (LNS)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane departed as the fifth airplane in a formation of six airplanes during an airshow demonstration and was about 75 feet to the trailing right of the preceding airplane during the takeoff and initial climb. The pilot reported that, about 10 feet above ground level (agl), the airplane drifted right of the runway centerline and that he then realigned the airplane with the centerline. About 35 feet agl, he encountered “severe turbulence,” and the airplane banked left uncontrollably. He attempted to regain control of the airplane; however, it stalled and subsequently impacted the ground in a nose-low attitude. A left crosswind of about 3 knots existed at the time of the accident. According to Advisory Circular 90-23F, “Aircraft Wake Turbulence,” “a crosswind will decrease the lateral movement of the upwind vortex.”
Postaccident examination revealed that the pitch trim was set in an almost full nose-up position. The pilot likely did not comply with the before takeoff checklist and confirm that the trim setting was at 0 before takeoff. In addition, the airplane likely encountered wake turbulence from the preceding airplane. The pilot reported no mechanical malfunction or abnormality that would have precluded normal operation.

Probable Cause: The pilot’s failure to control the airplane’s pitch attitude, which resulted in an aerodynamic stall during the initial takeoff climb. Contributing to the accident was the pilot’s failure to set the trim in accordance with the pretakeoff checklist and the airplane’s encounter with wake turbulence from a preceding airplane.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA13LA366
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB

Location

Media:

Revision history:

Date/timeContributorUpdates
20-Aug-2013 04:17 Geno Added
21-Aug-2013 08:48 harro Updated [Embed code]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
29-Nov-2017 08:58 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Embed code, Narrative]

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