Incident Scottish Aviation Bulldog 101 N101MY,
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ASN Wikibase Occurrence # 162264
 
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Date:Thursday 2 June 2011
Time:20:00
Type:Silhouette image of generic BDOG model; specific model in this crash may look slightly different    
Scottish Aviation Bulldog 101
Owner/operator:private
Registration: N101MY
MSN: BH100/166
Total airframe hrs:4815 hours
Engine model:Lycoming IO-360-A1B6
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Location:Chandler, AZ -   United States of America
Phase: En route
Nature:Private
Departure airport:Chandler, AZ (CHD)
Destination airport:Chandler, AZ (CHD)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that the engine surged and sustained a partial loss of engine power during a local night flight. He attempted to restore engine power, but was unsuccessful and made a forced landing to an open field where the airplane impacted a ditch, collapsing the landing gear and bending the firewall during the landing roll. The pilot said that the entire flight was performed with the fuel selector on the “BOTH” position and that when the engine first began to surge, the fuel gauges registered a quarter of capacity in each tank.

The fuel system consisted of inner and outer interconnected tanks in each wing, which supplied fuel through a non-return valve to a fuel selector, a filter, and a booster pump grouped together near the front left seat, then through the engine-driven pump to the injector unit. Unusable fuel in each wing is 0.5 gallons. Airplane recovery personnel said that no fuel was found in the left wing tanks and about 8 gallons of fuel were found in the right wing tanks, although the gear collapse may have allowed fuel to migrate from the high wing to the low wing. The airplane was examined and no fuel system discrepancies were found. The engine was test run in the airframe and it started and ran normally.
Probable Cause: A loss of engine power during cruise flight for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR11LA246
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
15-Nov-2013 09:57 Masen63 Added
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 16:54 ASN Update Bot Updated [Cn, Other fatalities, Departure airport, Destination airport, Source, Narrative]
30-Nov-2018 19:34 TB Updated [Aircraft type, Cn, Operator, Other fatalities]

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