ASN Wikibase Occurrence # 162799
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Date: | Wednesday 18 December 2013 |
Time: | 15:15 |
Type: | Piper PA-32-301 Saratoga |
Owner/operator: | Private |
Registration: | N8169C |
MSN: | 32-8006016 |
Year of manufacture: | 1980 |
Total airframe hrs: | 3031 hours |
Engine model: | Lycoming IO-540 SER |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Whiteman Airport (KWHP), Pacoima, Los Angeles, CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Los Angeles, CA (WHP) |
Destination airport: | Los Angeles, CA (WHP) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that, during the preflight inspection, he noted that the fuel gauges located on the wing tanks indicated that each tank contained about 12 gallons of fuel. After performing a run-up inspection, he completed one takeoff and full-stop landing. After taking off again, the pilot turned the airplane onto the crosswind leg of the traffic pattern, and the engine subsequently experienced a total loss of power. As the airplane began to lose altitude, the pilot switched the fuel selector from the right fuel tank to the left fuel tank position. The pilot unsuccessfully attempted to restart the engine and then maneuvered the airplane to a field to perform an emergency landing. While landing, the airplane’s landing gear dug into the soft terrain, and the nose landing gear collapsed, which resulted in damage to the firewall.
Maintenance personnel reported that, before transporting the wreckage to a storage facility, they removed about 10 gallons of fuel from the left wing tank and about 1 quart of fuel from the right wing tank; the fuel system was not breached, and no evidence of fuel leakage was found. During the postaccident examination, the engine was successfully started and run for over 5 minutes at various power settings. No mechanical anomalies were noted with the engine or airframe that would have precluded normal operation.
Probable Cause: The total loss of engine power during takeoff due to fuel starvation, which resulted from the pilot’s failure to adequately manage the fuel supply.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR14LA071 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=8169C Location
Revision history:
Date/time | Contributor | Updates |
19-Dec-2013 17:13 |
Geno |
Added |
02-Jan-2014 22:29 |
Geno |
Updated [Total occupants, Nature, Departure airport, Source, Damage, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 09:28 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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