Loss of control Accident Bowers Fly Baby 1A N6054Q,
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ASN Wikibase Occurrence # 165415
 
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Date:Friday 11 April 2014
Time:10:07
Type:Silhouette image of generic FB1A model; specific model in this crash may look slightly different    
Bowers Fly Baby 1A
Owner/operator:Private
Registration: N6054Q
MSN: 1068
Year of manufacture:2006
Total airframe hrs:32 hours
Engine model:Continental A65-8
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Near Mariposa-Yosemite Airport (KMPI), Mariposa, CA -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:Mariposa, CA (MPI)
Destination airport:Mariposa, CA (MPI)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The plans-built single-seat airplane had been constructed about 8 years before the accident by another individual, who had flown it about 30 hours before it was purchased by the current owner/pilot. In the year since the purchase, due to the low build-quality of the airplane, the pilot had made several modifications and repairs to the airplane. The accident flight was the pilot’s fifth flight in the airplane. Review of the pilot’s flight logbook indicated that his most recent flight review occurred about 7 years before the accident and that he had flown only 15 hours in the 2 years before the accident.
A witness reported that shortly after takeoff, when the airplane was about 3 miles from the airport, the engine began making a sound as if power was intermittently being interrupted. The nose of the airplane began to pitch up aggressively as it flew out of view. The wreckage location, wreckage distribution, and impact signatures indicated that the airplane struck the ground in a steep nose-low attitude, consistent with an aerodynamic stall event.
Postaccident examination of the carburetor revealed multiple maintenance-related discrepancies, any one of which could have resulted in the loss of engine power. Additionally, before the accident, the pilot reported to a friend that the airspeed indicator was not reliable and that the airplane exhibited roll control anomalies. Both of these conditions would have hindered the pilot’s ability to safely operate the airplane.

Probable Cause: The partial loss of engine power due to an improperly maintained carburetor and the pilot's subsequent failure to maintain aircraft control.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR14FA165
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=6054Q

History of this aircraft

Other occurrences involving this aircraft
20 October 2006 N6054Q Myron G Williams 0 Oakdale, California sub

Location

Revision history:

Date/timeContributorUpdates
11-Apr-2014 22:53 Geno Added
12-Apr-2014 00:07 Geno Updated [Aircraft type, Source, Narrative]
14-Apr-2014 23:02 Geno Updated [Registration, Cn, Operator, Source, Damage, Narrative]
29-Apr-2014 05:57 Geno Updated [Time, Phase, Nature, Departure airport, Destination airport, Source]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
29-Nov-2017 14:02 ASN Update Bot Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative]

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