Accident McDonnell Douglas DC-9-31 N1799U,
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Date:Friday 18 May 2007
Time:13:00
Type:Silhouette image of generic DC93 model; specific model in this crash may look slightly different    
McDonnell Douglas DC-9-31
Owner/operator:Northwest Airlines
Registration: N1799U
MSN: 47370/551
Year of manufacture:1971
Total airframe hrs:83094 hours
Engine model:Pratt & Whitney JT8D-9A
Fatalities:Fatalities: 0 / Occupants: 99
Aircraft damage: Substantial
Category:Accident
Location:Near Syracuse, NY -   United States of America
Phase: En route
Nature:Passenger - Scheduled
Departure airport:Syracus, NY (SYR)
Destination airport:Detroit, MI (DTW)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While at its departure airport, a Douglas DC-9-31’s baggage was loaded by contract ramp personnel. After departure, the airplane was climbing through approximately 20,000 feet mean sea level (msl), when the flight crew heard a "loud pop" and the cabin depressurized. The flight crew donned their oxygen masks and diverted to the closest airport in point of time, and landed uneventfully. Postflight inspection of the accident airplane revealed a 12-inch by 5-inch fuselage skin tear, approximately 6 feet forward of the forward cargo door. During the course of the investigation it was revealed that at some point during the aircraft luggage off-loading or loading process, the engine of the belt loader quit operating. The senior of three ground agents working the flight decided to move the belt loader away from the airplane by pushing the belt loader with a luggage tug; however, during the attempt to move the belt loader, the tug’s cab contacted the fuselage. The senior ground agent then advised “don’t say anything” to one of the other employees who was working the flight with him, and the airplane departed and later depressurized. The senior ground agent’s actions were contrary to published guidance in the company’s training handbook and operation manual.
Probable Cause: The senior ground agent's failure to follow written procedures and directives.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC07LA121
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070601X00676&key=1

Location

Revision history:

Date/timeContributorUpdates
19-Apr-2014 07:08 Katonk2014 Added
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
04-Dec-2017 18:39 ASN Update Bot Updated [Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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