ASN Wikibase Occurrence # 165856
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Date: | Friday 25 April 2014 |
Time: | 18:25 |
Type: | Piper PA-34-200 Seneca I |
Owner/operator: | United Flight Systems Inc |
Registration: | N56755 |
MSN: | 34-7450029 |
Year of manufacture: | 1973 |
Total airframe hrs: | 11348 hours |
Engine model: | Lycoming I0360 SER |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | David Wayne Hooks Memorial Airport (KDWH), Houston, TX -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Spring, TX (DWH) |
Destination airport: | Spring, TX (DWH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor was flying the airplane and demonstrating a short-field landing during the instructional flight. The flight instructor reported that, after the airplane touched down about 90 mph, the right brake pedal went full forward, and the brakes were not slowing the airplane. He pumped the brake pedal several times to build pressure in the lines but was not successful. The pilot receiving instruction checked his brake pedals and confirmed that the right brake was not working. The flight instructor then shut down both engines when the airspeed was about 60 mph and subsequently lost directional control of the airplane. The airplane then drifted off the left side of the runway and impacted a ditch, which resulted in substantial damage to the lower aft fuselage and lower forward empennage.
An examination of the brakes the day after the accident did not reveal any problems with the right brake; however, it could not be determined whether the brake system had been serviced or repaired following the accident. A photograph of skid marks on the runway showed that the skid marks for the left main landing gear (MLG) tire seemed to be darker than the skid marks for the right MLG tire. The evidence indicates that the right brake likely lost effectiveness during the landing, which resulted in a loss of directional control; however, the reason for the brake’s loss of effectiveness could not be determined.
Probable Cause: The loss of right brake effectiveness during landing for reasons that could not be determined based on the available evidence, which resulted in a loss of directional control.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14LA220 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=56755 Location
Revision history:
Date/time | Contributor | Updates |
29-Apr-2014 04:05 |
Geno |
Added |
02-May-2014 22:24 |
Geno |
Updated [Time, Operator, Nature, Departure airport, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 14:03 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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