ASN Wikibase Occurrence # 166035
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Date: | Tuesday 6 May 2014 |
Time: | 11:18 |
Type: | Lancair 360 Mk II |
Owner/operator: | Private |
Registration: | N246AK |
MSN: | 778 |
Year of manufacture: | 1999 |
Total airframe hrs: | 790 hours |
Engine model: | Lycoming IO-360-B1E |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Field in Stephenson, west of Crivitz, WI -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Oconto, WI (OCQ) |
Destination airport: | Iron Mountain, MI (IMT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, about 10 to 15 minutes after takeoff in the single-engine airplane, he smelled fuel in the cockpit, and the airplane's fuel pressure gauge read 0. He activated the electric fuel boost pump, but the fuel pressure reading remained 0. At this point, the engine lost power, and the pilot subsequently executed a wheels-up forced landing to a field.
Postaccident examination of the airplane revealed that the inlet hose to the mechanical fuel pump was not connected; the hose fitting and the fuel pump’s mating fitting were not damaged. Based on the available evidence, it is likely that the hose fuel fitting was not properly installed, which allowed the fitting to vibrate loose during operation until it became disconnected and resulted in the loss of engine power due to fuel starvation. Because the hose fitting was found higher than the fuel tanks, fuel would not have leaked from the hose while the airplane was parked. Therefore, the pilot would not have been able to detect the discrepancy during preflight examination of the airplane.
Probable Cause: The improper installation of the hose fuel fitting, which resulted in the fitting becoming disconnected and the subsequent loss of engine power due to fuel starvation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14LA241 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=246AK Location
Revision history:
Date/time | Contributor | Updates |
06-May-2014 20:35 |
Geno |
Added |
30-May-2014 17:13 |
Geno |
Updated [Nature, Departure airport, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 14:22 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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