ASN Wikibase Occurrence # 166127
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Date: | Saturday 10 May 2014 |
Time: | 15:45 |
Type: | Cessna T207A Turbo Stationair 7 |
Owner/operator: | American Aviation Inc |
Registration: | N7311U |
MSN: | 20700395 |
Year of manufacture: | 1977 |
Total airframe hrs: | 14883 hours |
Engine model: | Continental. TSIO-520-GCM |
Fatalities: | Fatalities: 1 / Occupants: 7 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Page Municipal Airport (KPGA), Page, Arizona -
United States of America
|
Phase: | Landing |
Nature: | Survey |
Departure airport: | Page, AZ (PGA) |
Destination airport: | Page, AZ (PGA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During a local sightseeing flight, the pilot noticed that the engine had lost partial power, and he initiated a turn back toward the airport while troubleshooting the loss of power. Despite the pilot’s attempts, the engine would not regain full power and was surging and sputtering randomly. The pilot entered the airport’s traffic pattern on the downwind leg, and, while on final approach to the runway, the airplane encountered multiple downdrafts and wind gusts. It is likely that, due to the downdrafts and the partial loss of engine power, the pilot was not able to maintain airplane control. The airplane subsequently landed hard short of the runway surface and nosed over, coming to rest inverted. The reported wind conditions around the time of the accident varied between 20 and 70 degrees right of the runway heading and were 14 knots gusting to greater than 20 knots. In addition, a company pilot who landed about 8 minutes before the accident reported that he encountered strong downdrafts and windshear while on final approach to the runway and that he would not have been able to reach the runway if he had a partial or total loss of engine power.
Postaccident examination of the airframe and engine revealed no evidence of any preexisting mechanical malfunctions or failures that would have precluded normal operation. The engine was subsequently installed on a test stand and was successfully run through various power settings for several minutes. The reason for the partial loss of engine power could not be determined.
Probable Cause: The pilot’s inability to maintain aircraft control due to a partial loss of engine power and an encounter with downdrafts and gusting crosswinds while on final approach to the runway. The reason for the partial loss of engine power could not be determined because postaccident examination revealed no mechanical malfunction or failure that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR14FA186 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=7311U Location
Revision history:
Date/time | Contributor | Updates |
11-May-2014 07:22 |
Útila |
Added |
11-May-2014 07:22 |
harro |
Updated [Registration] |
11-May-2014 07:23 |
harro |
Updated [Date] |
12-May-2014 00:29 |
Geno |
Updated [Time, Aircraft type, Registration, Cn, Operator, Location, Nature, Departure airport, Destination airport, Source, Damage] |
17-May-2014 00:25 |
Geno |
Updated [Time, Operator, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
28-Feb-2017 07:42 |
PiperOnslaught |
Updated [Source, Narrative] |
29-Nov-2017 14:24 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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