ASN Wikibase Occurrence # 167870
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Date: | Friday 11 July 2014 |
Time: | 14:19 |
Type: | Mooney M20M TLS |
Owner/operator: | Gilliland William M |
Registration: | N72FG |
MSN: | 27-0118 |
Year of manufacture: | 1991 |
Total airframe hrs: | 1823 hours |
Engine model: | Lycoming TI0-540 SER |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Greenwood Municipal Airport (KHFY), Indianapolis, Indiana -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Greenwood, IN (HFY) |
Destination airport: | Longview, TX (GGG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot and flight instructor were repositioning the airplane for an annual inspection, and the private pilot planned to receive instrument flight training during the trip. Witnesses reported that the engine sounded good as the airplane taxied to the runway and during the engine run-up. However, several witnesses reported observing blue smoke trailing the airplane at the beginning of the takeoff and hearing the engine "popping" and "misfiring." The airplane was 50 to 100 ft above the ground and about one-quarter of the way down the 5,100-ft-long runway when its nose lowered slightly. Witnesses stated that they thought the pilot was going to land the airplane back on the remaining runway, but the airplane's nose then rose, and the airplane continued climbing. The airplane was described as being slow and "wallowing," with the nose pitching up and down slightly as it continued to climb to a maximum altitude of about 100 to 150 ft above the ground. The right wing dropped, and the airplane descended, contacting a garage and two houses before coming to rest in a residential backyard where a postimpact fire ensued. A postaccident examination of the airplane, engine, and engine components did not reveal any anomalies that would have precluded normal operation.
Probable Cause: A partial loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation. Also causal to the accident was the pilots' decision to continue the takeoff despite early indications of engine anomalies.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14FA356 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=72FG Location
Media:
Revision history:
Date/time | Contributor | Updates |
11-Jul-2014 19:06 |
harro |
Added |
11-Jul-2014 19:17 |
Anon. |
Updated [Aircraft type, Total occupants, Embed code, Narrative] |
11-Jul-2014 20:07 |
Geno |
Updated [Time, Aircraft type, Registration, Cn, Operator, Location, Phase, Departure airport, Source, Narrative] |
12-Jul-2014 06:46 |
gerard57 |
Updated [Total fatalities] |
18-Jul-2014 01:05 |
Geno |
Updated [Time, Nature, Destination airport, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 18:52 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Embed code, Narrative] |
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